Andrews Shafter Lake Means 10/27/2015

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1 Andrews Shafter Lake Means 10/27/2015 Status this A.M.: Circulate hole clean with 2% KCL 12 Basic Well Service MIRU Unloaded Racks / Catwalk / BOP equipment. Racked and tallied 56 joints 2 7/8" L-80 tubing and 150 joints 2 7/8" PH-6 tubing. Removed Well head cap and installed BOP equipment. TIH with a 4 3/4" bit on 150 joints 2 7/8" PH-6 and 32 joints 2 7/8" L-80 tubing tagging 5642' 12 C.I. AFE AMOUNT $0.00 $200/hr

2 Andrews Shafter Lake Means 10/28/2015 Status this A.M.: pressure test 5 1/2" casing to 6000 psi 11 Kinney Pump Truck RU on 2 7/8" tubing and displaced wellbore with 225 bbls 2% KCL water clearing well of debris. TOH with 32 joints 2 7/8" L-80 tubing, 150 joints 2 7/8" PH-6 tubing and 4 3/4" bit. Removed BOP, Oil States field service measured wellhead for stinger. Epic Wireline Service RU on 5K flange, ran two passes with CBL from 4770' - 50'. 1st pass with CBL at 0 psi and 2nd pass with 1000 psi applied to 5 1/2" casing. Found cement 2800'. RD wireline equipment, installed BOP, Oil States Service RU and stung into Well head equipment profile. 13 C.I. AFE AMOUNT $0.00 $200/hr

3 Andrews Shafter Lake Means 10/29/2015 Status this A.M.: Continue TIH with Bit 12 Petro Plex Pump MIRU, Tested lines to 7000 psi. loaded hole with 2 bbls KCL, pressure tested the 5 1/2" Casing to 6000 psi and charted for 15 minutes. Held pressure OK. Petro Plex RDMO, Oil States stung out of Well Head and removed from BOP. DOC's Reverse Unit Equipment arrived on location and RU. TIH with a 4 3/4" Plug Muncher on 150 joints 2 7/8" PH-6 and 32 joints 2 7/8" L-80 tbg. Tagged up at 5642', RU Swievel, broke circulation with 2% KCL and drilling on PBD for 1.5 hours without making any hole. Decided to pull and replace Plug Muncher with 4 3/4" Tri Cone Bit.RD Swievel, TOH with 2 7/8" L-80 and PH-6 tubing. TIH with a 4 3/4" Bit on 60 joints 2 7/8" PH-6 tubing - shut down due to darkness. 12 C.I. AFE AMOUNT $0.00 $200/hr

4 Andrews Shafter Lake Means 10/30/2015 Status this A.M.: Perform step rate test. 13 Continued TIH with 90 joints 2 7/8" PH-6 and 33 joints 2 7/8" L-80 tubing, tagging bottom now at 5681'. RU Reverse Unit Equipment, broke circulation and drilled up Wiper Plug Rubber / Wipper plug and Cement down to 5710'. Circulated bottoms up, pressure tested ( attempting to establish Rate ) to 2000 psi.held pressure for ~ 5 min. Lowered bit back to bottom, continued to drill at a very slow rate to 5716' getting returns of small hard metal & Cement. Circulated bottoms up, established rate of 4.5 bpm / 200 psi. RD DOC's Reverse Unit equipment, TOH with 150 joints 2 7/8" PH-6 and 34 joints 2 7/8" L-80 tubing. 11 C.I. 24 C.I. 24 C.I. AFE AMOUNT $0.00 $200/hr

5 Andrews Shafter Lake Means 11/2/2015 Status this A.M.: Prepare for FRAC 11 Cudd Energy Services MIRU, loaded pumps with 2% KCL, began pumping 3.5 bpm / 0 psi. loaded hole with 54 bbls KCL pumped. Dropped rate to 2 bpm and began Step Rate test. Results are as follows : 2 bpm / 300 psi / 10 bbls pumped 4 bpm / 600 psi / 20 bbls pumped 6 bpm / 714 psi / 20 bbls pumped 8 bpm / 900 psi / 20 bbls pumped 10 bpm / 1150 psi / 20 bbls pumped 12 bpm / 1267 psi / 20 bbls pumped ISIP psi / 5 min. 0 psi RD Cudd, TIH with 150 joints 2 7/8" PH-6, 32 joints L-80 tubing and laid down all pipe in singles on Pipe Rack. Removed BOP and installed FRAC Valve. RD Pulling Unit 13 C.I. AFE AMOUNT $0.00 $200/hr

6 Andrews Shafter Lake Means 11/4/2015 Status this A.M.: Begin Stage 1 frac 6:00 20:00 14 MIRU wireline equipment and Oil States isolation equipment. MIRU Schlumberger frac equipment and spot in flowback manifold. Test lines to 7500 psi OK. Shut down and begin frac with daylight crew. 20:00 6:00 10 CI $0.00 AFE AMOUNT $0.00 J BRYANT

7 Andrews Shafter Lake Means 11/5/2015 Status this A.M.: Perforate Stage 16 6:00 6:00 24 Prime pumps and held safety meeting. Pumped 1,350,644# 20/40 sand in 549,271 gals of 20# X-linked gel and lb Broadband pills. AIR psi TP. Prepare to run depth correlation pass with wireline. $0.00 AFE AMOUNT $0.00 J BRYANT

8 Andrews Shafter Lake Means 11/6/2015 Status this A.M.: Prepare to clean out plugs 6:00 22:00 16 Run wireline correlation pass. Found short jt at 3695' and DV tool at 5692'. TOH and pick up plug and gun assembly. Pump tools down and set plug at 5703'. Perforated Stage 16 perfs at 5,673', 5,568', and 5,459' and TOH. Pumped Stage 16 with 270,040# 20/40 sand and 111,568 gals 20# X-link gel. AIR 62 bpm at 3634 psi. Pumped down Stage 17 assembly and set plug at 5394'. Perforated Stage 17 perfs at 5,038', 5,165', and 5,292' and TOH. Pumped Stage 17 with 270,640# 20/40 sand and 112,460 gals 20# X-link gel. AIR 61 bpm at 3242 psi. Pumped down Stage 18 assembly and set plug at 5,013'. Perforated Stage 18 perfs at 4,911', 4,784', and 4,657'. Pumped Stage 18 with 270,480# 20/40 sand and 113,162 gals 20# X-link gel. AIR psi. RD frac equipment and Oil States. RDMO water transfer. RU flow back and open well with 0 psi. Released flowback and left well open to pit. 22:00 6:00 8 CI $0.00 AFE AMOUNT $0.00 J BRYANT

9 Andrews Shafter Lake Means 11/10/2015 Status this A.M.: RU Foam Unit 12 Basic Well Service MIRU Unloaded Racks / Catwalk / BOP equipment. Racked and tallied 56 joints 2 7/8" L-80 tubing and 150 joints 2 7/8" PH-6 tubing. Removed FRAC Valve and installed BOP equipment. TIH with a 4 3/4" Plug Muncher on 150 joints 2 7/8" PH-6 and 11 joints 2 7/8" L-80 tubing tagging Top 4993'. RU DOC's Reverse Unit, worked to break circulation with 540 bfw pumping at 3.5 bpm / 320 psi. Appears to be pumping into top FRAC Zone. Laid down Swievel Equipment / Pulled 36 joints tubing placing EOP above Curve. 12 C.I. AFE AMOUNT $0.00 $200/hr

10 Andrews Shafter Lake Means 11/11/2015 Status this A.M.: Continue clean out 6 Returned to location with Basic Foam Unit, RU - FU on 2 7/8" tubing, loaded Blender with FW and began pumping 2.5 ppg Solvent / Soap / Inhibitor down the 2 7/8" 3 bpm / 50 psi. Recovering Foamy Oil / water mixture to pit. Shut pump down, lowered Plug Muncher down hole, tagging top plug at 4993'. RU Swivel, broke circulation and drilled up first plug in approx. 45 minutes. Circulated bottoms up. While breaking Swivel off, Sandline on Pulling Unit broke just below Rope Socket. Deployed Basic Crew from Denver City, Texas for repair. 2 Waiting for repair crew. 6 Repaired Rope Socket on Workover Rig, continued in hole with BHA and tagged partially cut up Plug at 5136'. ~238' above second Plug. Picked up Swivel and started up FU. Began pumping Foam down hole breaking circulation with 50 bbls pumped away. Stripper Head atop BOP began to leak forcing operations to Shut Down. Replaced Stripper Head Rubber, pulled up above top perf and circulated hole clean. 10 C.I. AFE AMOUNT $0.00 $200/hr

11 Andrews Shafter Lake Means 11/12/2015 Status this A.M.: Clear location for Coil Tubing Unit 14 Returned to location, RU Basic Foam Unit and began pumping Foam mixture / air breaking circulation w/ approx. 25 bbls fluid. Cleared 5 1/2" casing with ~20 bbls foam. TIH with 2 7/8" PH-6 / 2 7/8" L-80 tubing and re-tagged obstruction at 5136'. Began initiating Foam at max rate ( 4 bpm ) 1350 psi, working to break circulation. Broke a slight amount of circulation ( small blow ) after one hour. Continued Foam circulation and pipe became stuck. Worked approx. 1 hour working pipe / pumping Foam to free up tubing. Broke off Swivel, TOH laying 2 7/8" tubing on rack / pipe became stuck again at 4739'. Worked pipe free in about 1.5 hours, continued TOH laying down all L-80 / PH-6 tubing / BHA on racks. Removed BOP and installed Frac Valve. RD both Foam Unit and Reverse Unit and removed from location. 10 C.I. AFE AMOUNT $0.00 $200/hr

12 Andrews Shafter Lake Means 11/13/2015 Status this A.M.: RU Coil Tubing Unit 12 Basic Well Service RDMO Loaded Workstring onto road float / Stacked Racks and Catwalk off location. Loaded Three 500 bbl Frac Tanks with FW / Unloaded and set up Flow Back Manifold / Slug Catcher and Gas Buster. 12 C.I. 24 C.I. 24 C.I. $0.00 AFE AMOUNT $0.00

13 Andrews Shafter Lake Means 11/16/2015 Status this A.M.: Begin clean out w/ Coil Tubing 24 Coil Tubing Services MIRU. C.I $0.00 AFE AMOUNT $0.00

14 Andrews Shafter Lake Means 11/17/2015 Status this A.M.: Clear location / RU Pulling Unit 19.5 Coil Services Picked up Lubricator / installed Butterfly Mill on end of Coil, Tested Lubricator / Lines / 3000 psi. All held OK. TIH with Coil / Tools at 60' per minute, Broke circulation with a blend of 400 /1 of Nitrogen / Water / Foamer / and Friction Reducer. Engaged Plug #1 at 5382', Drilled up in 20 minutes. Lowered Coil / Mill and tagged 2nd 5382'. Drilled up Plug with a avg. blend of 300 / 2.5 and cleared plug in 2 hours of drilling. Lowered Mill ~150' and began loosing returns. Changed blend to 500 / 1.5 but unable to recover steady returns. Began TOH w/ Coil and lost total returns. TOH to top of curve, pulling 7' / min., increased pull speed to 60' / min., regained full 2600'. Circulated 2 x bottoms up, TIH with Coil / 700 / 1.3 blend. Tagged Third 5701'. Drilled up Plug in 22 minutes, and tagged PBD ( junk in hole ) at 5703'. Circulated 2x bottoms up, TOH with Coil and BHA. Laid down tools and RD Coil Unit. 4.5 C.I. $0.00 AFE AMOUNT $0.00

15 Andrews Shafter Lake Means 11/18/2015 Status this A.M.: Install Sub Pump Equipment 8 Schlumberger Coil Services moved all equipment off location. Found well with 150 psi., bled gas pressure down to 0 psi through Manifold. Unflanged Slug Catcher and Blow down Manifold from well and removed from location. Basic Rig Service MIRU Removed Frac Valve, installed new 3K x 8 5/8" Adaptor Flange on top of 7 1/16" x 5 K Tubing spool. Landed BOP and Closed in Blind Rams. Set up Pipe Racks / Catwalk. Unloaded Racked and tallied 129 Joints 2 7/8" EUE/8rd J-55 Tubing IPC w/ TK C.I. AFE AMOUNT $0.00 $200 / hr

16 Andrews Shafter Lake Means 11/ Status this A.M.: Tie well into Flowline 14 Schlumberger Services ( Pump / Spooler ) MIRU Picked up 5 joints 2 7/8" Fiberglass tubing w/ bottom tube plugged ( Cavity ), Cavins 27/40 Desander and assembled Sub pump equipment. Schlumberger Service Tech serviced and checked all equipment after assembly, TIH with sub equipment, on 116 joints 2 7/8" tubing ( all tubing are EUE / 8rd J-55 IPC ) Removed BOP, and made bottom Pigtail splice. Landed Hanger inside Flange Adaptor, Discovered top SS Nipple cut 2" short, not allowing enough room for Master Valve. Ordered new Nipple to be cut and should have delivery A.M. Installed temporary nipple / valve and started well up to pit. Pump up time was 5 min. / 965 SBHP / 45 hz / 36 amps. 10 C.I. AFE AMOUNT $0.00 $200 / hr

17 Andrews Shafter Lake Means 11/20/2015 Status this A.M.: Producing To Battery DFR 5 Gang Built 2" run and hooked well up to Flowline. Basic Well Service RDMO Started up 48 HZ / 40 AMPS / 910 PIP. Pump up time ~30 seconds. Adjusting FWKO at JV-14 Battery Detail of Sub breakdown as follows: 2 Pumps - D3500N CR-CT / 89 stages/ SN 2FM5F29015, 89 stages 2FM5F29144 and AGH, D20-60 C-CT / SN 8DM5J Intake ( VGSA D20-60 ) SN 4BB5H / Protector MAX LSBPB -S-LT w/ SN 3CM , 270 HP Motor 456 series 2676 VLT / 67.1 AMP Pressure instrument type XT150 Type 0 w/ SN S103XB15N Producing to Battery 24 Producing to Battery 24 Producing to Battery AFE AMOUNT $0.00 $200 / hr