EPRI-EPA-DOE-A&WMA Power Plant Air Pollutant Control MEGA Symposium

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Paper # 72 CCS Project with Alstom s Chilled Ammonia Process at AEP s Mountaineer Plant EPRI-EPA-DOE-A&WMA Power Plant Air Pollutant Control MEGA Symposium R Bollinger D Muraskin August 31, 2010 Baltimore, MD

Presentation Outline Project Overview CO 2 Storage Characterization & Design CO 2 Storage System Operations Alstom Chilled Ammonia Process Conclusions Q&A MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 2

Project Overview Mountaineer Plant (WV) Flue gas Utilities Alstom Chilled Ammonia/ CO 2 Capture Pipeline & Secondary Compression CO 2 Storage (Battelle) MMV Goals for the Project Validate Alstom s Chilled Ammonia Process Integration with CO 2 Sequestration Longer term characterization of storage reservoirs Flue Gas Slip Stream from Mountaineer Plant Equivalent to 20 MW (electric) from WFGD System Capture and Store ~100k metric tons of CO 2 per year Project Milestones Started engineering, planning, & permitting 3Q 2007 Started construction 2Q 2008 Captured CO2 for first time Sep 1 2009 Injected CO2 for first time Oct 1 2009 2 Injection Wells / 3 Monitoring Wells MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 3

Site Characterization Study Site characterization and feasibility assessment conducted in 2003 by Battelle & Others under DOE funded project Foundational work for AEP s CCS program Identified Two(2) feasible injection formations for CO 2: Rose Run Sandstone (AEP-2, 7800 ft) Copper Ridge B Zone (AEP-1, 8200 ft) Characterization study found thousands of feet of Cap Rock to contain the stored carbon dioxide Seismic Survey Summer 2003 Drilling and Testing AEP#1 Well 2003-05 MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 4

Injection Well Design Well Design an important means to contain CO 2 in reservoir Ex. AEP-2 in Rose Run Sandstone Similar in design to wastewater injection wells used in oil & gas industry Type V Underground Injection Control permit issued by WVa DEP Multiple cascading well casings, to provide isolation from: Shallow freshwater Intermediate zones containing coal seams, oil & natural gas Stainless steel casing and CO 2 resistant cement deep injection well section MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 5

Full Core Samples 2003 Characterization Study Rose Run Sandstone- 116 ft total thickness, 30 ft porous sandstone Full Rock Core 7762-7772 Full Rock Core 7772-7782 Full Rock Core 7818-7828 Hydraulic Core Tests 7763.5 ft Lithology = Sandstone Density = 2.68 g/ml Porosity = 9.1% Permeability = 36 md Hydraulic Core Tests 7775 ft Lithology = Sandstone Density = 2.64 g/ml Porosity = 10.4% Permeability = 49 md Hydraulic Core Tests 7819 ft Lithology = Sandstone Density = 2.63 g/ml Porosity = 11.5% Permeability = 36 md Data from Battelle Porosity & Permeability suggested adequate storage reservoirs MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 6

Cap Rock Sidewall Cores 2003 Characterization Study Rotary Sidewall Core 7275 ft Beekmantown Dolomite 7210-7755 ft Thin Section 7275 ft Wireline Log 7100-7300 7300 ft Feet Battelle Graphic 0 2 4 cm X100 Hydraulic Core Tests 7275 ft Lithology = Dolomite Density = 2.82 g/ml Porosity = 0.38% Permeability = <0.001 md Shows Consistent Lithology Shows Dolomite Lithology Shows High Density and Very Low Porosity MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 7 Data from Battelle Low Porosity & Permeability indicate excellent cap rock to maintain CO2 storage

Well Monitoring System Injection Well Monitoring A - Flow rate, pressure, temperature - Annulus pressure - Corrosion monitoring -CO 2 product analysis Surface Leak Detection Methods B Shallow groundwater monitoring CO2 Tracking and Caprock / Confining Layer Monitoring Methods C Fluid sampling D Wireline logging E Pressure monitoring F Cross-well seismic survey Battelle Graphic MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 8

Storage System Operations Injectivity better than expected into AEP-1 Copper Ridge formation AEP-2 Rose Run slow to respond initially; better response recently Testing & Monitoring have confirmed CO 2 containment Next steps- To evaluate longer term reservoir behavior / storage capacity MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 9

Presentation Outline Project Overview CO 2 Storage Characterization & Design CO 2 Storage System Operations Alstom Chilled Ammonia Process Conclusions Q&A MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 10

CO 2 Capture Technologies SOLUTIONS DEVELOPED BY ALSTOM Post -combustion (New+retrofit) Oxy-combustion (New + retrofit) Pre-combustion (New only) Oxy-combustion (New + retrofit) Post-combustion (New + retrofit) -Chilled Ammonia Process -Advanced Amines -Anti-Sublimation Source: Vattenfall Source: Vattenfall MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 11

Chilled Ammonia Process Technology Features Energy efficient capture of CO 2 Utilizes ambient conditions / natural sources for flue gas cooling Can accommodate typical flue gas contaminants (SO x, HCl, HF, NO x ) Flue gas exhaust conditions suitable for release to atmosphere low ammonia slip additional testing forthcoming High pressure regeneration High purity CO 2 product, low moisture and ammonia Reduced CO 2 compressor power Lower regeneration energy, low vaporization of water from solvent Low cost and market stable reagent with potentially salable byproduct (ammonium sulfate) stream AEP Mountaineer Product Validation Facility Chilled Ammonia Process New Haven, WV MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 12

2006 CAP Development Program Summary Development Plan 2007 2008 2009 2010 2011 2012 2013 2014 2015 1 Small-bench (SRI completed) First technical hypothesis CALENDAR YEARS & DATES 2 Large-bench (SRI completed) Optimize absorber design for pilot 3 Field pilots - 15 000 TPY range WE Energies - 5MWth - coal E.On Karlshamn - 5 MWth oil/gas Validate key performance parameters WE test completed 4 Validation pilot 100 000 TPY range AEP Mountaineer 54 MWth - coal System reliability Coal and gas validation Statoil Hydro Mongstad Validation (40 MWth) - gas 5 FEED Large Scale Demonstration - 1 to 1,5 M TPY (400-800 MWth) Commercial Deployment in 2015 MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 13

CAP Development Program We Energies Field Pilot Field Pilot Program Operational June 2008 7700+ hours of operation on flue gas from PRB coal through completion of program in Oct 2009 Proof of Concept technology validation: 90% CO 2 capture efficiency NH 3 slip from DCC2 (~5 ppm) 99 + % CO 2 purity; <10 ppm NH 3 ; < 2,000 ppm H 2 O Functional unit operations Confirmation of process design tools CO 2 Field Pilot at Pleasant Prairie MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 14

CAP Development Program E.ON Karlshamn Field Pilot Karlshamn Power Plant (Sweden) CAP Field Pilot Field Pilot Program Operational Apr 2009 1500+ hours of operation on flue gas from sulfur fuel oil ongoing Proof of Concept technology validation: 90% CO 2 capture efficiency Flue gas NH 3 slip (~5 ppm) 99 + % CO 2 purity; <10 ppm NH 3 ; < 2,000 ppm H 2 O Functional unit operations Confirmation of process design tools MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 15

Location Capacity Size CO 2 Capture Efficiency CO 2 Storage AEP Mountaineer Product Validation Facility New Haven, WV 100,000 tonnes CO 2 /yr 110,230 tons CO 2 /yr 275 tonnes / day ~ 20 MWe 50,584 scfm 75% Deep geological formations CO2 Product CO 2 : 99.5+% H 2 O: 600 ppmv Upstream APC Equipment ESP, WFGD, SCR,SO 3 Mitigation Start-Up September 1, 2009 Fuel Bituminous Coal Reagent Ammonium bicarbonate \ carbonate Absorber Packing Column Regeneration Energy Byproduct Steam turbine extraction. Integration of steam condensate not included Ammonium sulfate Alstom s Chilled Ammonia Process at AEP s Mountaineer Plant, All pictures of the Mountaineer CO 2 Capture and Storage Project are the property of Alstom Power and/or AEP MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 16

AEP Mountaineer PVF Project Commissioning and Start-Up Experience The following CAP issues were identified during initial operation resulting in modifications to improve operability Utilization \ handling of solid reagent Operation of flue gas cooling coils Turndown of refrigeration system and CO 2 compressor Regenerator feed solution heat exchanger network Adjustments to accommodate transient power plant operation MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 17

AEP Mountaineer PVF Project Operating Summary CO 2 Captured CO 2 Injected PVF operating hours: 4400+ PVF capacity: 40-75% CO 2 captured: 19,000+ metric tons CO 2 injected: 14,000+ metric tons MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 18

AEP Mountaineer PVF Project Operating Data CO 2 removal efficiency above design value of 75% Flue gas measurements taken from on-line FTIR instrumentation Values verified by mass balance, existing plant CEMS, and field measurements Operating data reflects measurements at various conditions, reduced capacity Conditions shown include variations in scrubbing solution strength and plant capacity MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 19

AEP Mountaineer PVF Project Operating Data High purity CO 2 product purity achieved on a consistent, stable basis Measurements obtained from on-line FTIR analyzer, consistent with field measurements Reported CO 2 purity obtained by difference from H 2 O and NH 3 measurements Product CO 2 Purity (vol%) Date & Time MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 20

AEP Mountaineer PVF Project Operating Data Flue gas ammonia concentrations leaving the CAP maintained at low levels Flue gas ammonia measurements obtained using on-line FTIR Initial on-line instrument inconsistent with field measurements Sample port modifications made to improve on-line accuracy Modifications to instrument sample ports MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 21

AEP Mountaineer PVF Project Validation Program Main objectives to be demonstrated in test campaign and validated with EPRI Energy consumption CO 2 removal efficiency CO 2 product quality System reliability MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 22

Conclusion The Chilled Ammonia Process has been operated at the bench scale, pilot and validation facilities. The plants have demonstrated: CO 2 removal efficiency of 90%+ High purity CO 2 product (99.5%+) Storage of CO 2 in geological formations Ammonia emissions in the flue gas at desired levels Next steps for the AEP Mountaineer PVF Implementation, tuning of modifications to achieve continuous, full load operation Data collection and evaluation Performance validation with EPRI AEP \ Alstom engaged in DOE funded commercial scale plant project MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 23

Co-Authors Mike Hammond Project Engineer American Electric Power 1 Riverside Plaza Columbus, OH 43215 USA Brian Sherrick Project Manager American Electric Power 1 Riverside Plaza Columbus, OH 43215 USA Gary Spitznogle Chemical Engineering Manager American Electric Power 1 Riverside Plaza Columbus, OH 43215 USA Mike Varner Alstom Power, Inc. Project Manager 1409 Centerpoint Blvd Knoxville, TN 37932 USA Fred Kozak Alstom Power, Inc. Business Manager CAP Technology 1409 Centerpoint Blvd Knoxville, TN 37932 USA Matt Cage Alstom Power, Inc. Project Engineer 1409 Centerpoint Blvd Knoxville, TN 37932 USA MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 24

Presentation Outline Project Overview CO2 Storage Characterization & Design CO2 Storage System Operations Alstom Chilled Ammonia Process Conclusions Q&A MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 25

www.alstom.com

CAP Development Program AEP Mountaineer Product Validation Designed to capture 100,000 tonnes CO 2 /year Captured CO 2 is sequestered into two wells on the plant property Commenced engineering and permitting in Sep 2007 Started construction 2Q 2008 First CO 2 captured 1 st of September, 2009 Injection started 1 st of October, 2009 Technology Validation Program initiated with EPRI Alstom s Chilled Ammonia Process at AEP s Mountaineer Plant, All pictures of the Mountaineer CO 2 Capture and Storage Project are the property of Alstom Power and/or AEP MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 27

CAP Development Program We Energies Operating History 1 2 3 4 5 Total operating hours through Oct 30, 2009: 7,717 6 7 8 9 Total operating hours - 7,717 Over 65% Availability MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 28 1. Planned outage to support pilot modifications 2. Power Plant Forced Outage 3. Planned outage to support pilot modifications 4. Thanksgiving + Planned outage to support modification 5. Christmas Holidays 6. Power Plant Forced Outage 7. Planned outage for pilot maintenance 8. Unplanned outage for pilot maintenance (chiller) 9. Unplanned outage for pilot maintenance (stripper) 10. Planned outage to support pilot modifications 11. Outage Regenerator Level Transmitter 10 11

CAP Development Program Main Partnerships & Projects Portfolio Pleasant Prairie, WI (US) Coal 5 MWt Operational Jun08 to Oct09 Karlshamm (Sweden) Oil/Gas 5 MWt Operating since fall 2008 Chilled Ammonia Mountaineer WV (US) Coal Mongstad (Norway) Gas 54 MWt 40 MWt Operational since Sept 09 Engineering on going Pioneer (Canada) Coal >150MWe Planned start-up 2015 Commercial scale (US) Coal >200MWe Planned start-up 2015 Pilots in operation Tests completed * Project will include carbon sequestration Projects in different regions with different fuels MEGA Symposium CCS Project with Alstom s CAP at AEP s Mountaineer Plant August 31, 2010 - P 29