Grandville CWP Egg Shaped Anaerobic Digester and Bio-gas Cogeneration. Presented by: Brian Hannon, P.E., Moore & Bruggink

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Transcription:

Grandville CWP Egg Shaped Anaerobic Digester and Bio-gas Cogeneration Presented by: Brian Hannon, P.E., Moore & Bruggink

Outline Brief Project Background Why ESD ESD Startup Cogeneration System Energy Management Current Performance vs. Design Lessons Learned

City of Grandville Overview Grand Rapids US 196 Grandville 131

Customer Community Overview Ottawa County Georgetown Hudsonville Jamestown Jenison Blendon

Grandville Clean Water Plant

Grandville Clean Water Plant

Why Egg Shaped Anaerobic Digester (ESD)? Process Footprint Cost (life cycle) Cleaning Efficiency Client Comfort Ability to go to Class A

ESD Pipe Gallery

Anaerobic Digestion Relatively Simple Known Technology Produces two beneficial products w/ low energy input

How the ESD Works:

How the ESD Works:

How the ESD Works:

How the ESD Works:

Micro-Digestion Style Startup Good Seed Sludge starts the process Complete Control Process Allowed to Acclimatize No loss of Bio-Mass Steady State Operation Quickly Alkalinity Builds Quickly Temperature Control

Complete Mixing = Better Digestion = More Biogas! (and no periodic cleaning!)

Grandville s Biogas Components

Why Biogas Cleaning? Biogas Impurities Moisture H2S Siloxanes

Siloxane Damage to Boiler Silica Layer ½ to 1 Thick Pitting of Boiler Tubes

Siloxane Damaged Valve

Cogeneration System Dual Fuel (bio-gas and natural gas) - 280 kw using Bio-gas, - 360 kw using Nat Gas Internal exchangers to capture heat from engine cooling jacket and exhaust Efficiency of 86%

Power

Heat

Integrated Energy Management System (IEMS) ESD Biogas Supply ESD Heat Demand CHP Biogas Demand CHP Heat Supply CHP Power Supply System Power Demand Lab/Ops Heat Demand

Biogas Production Biogas Quantities Currently producing ~120,000 cuft/day Distribute between cogen, flare, and boiler

Power & Heat Production 70,000 CF/day Biogas to CHP Biogas Energy Content ~ 640 BTU/CF Average Energy Demand ~ 175 kw ~ $100,000 / year (@ $0.065/kWhr) Electrical Efficiency 32%

Power & Heat Production 70,000 CF/day Biogas to CHP Biogas Energy Content ~ 640 BTU/CF Average Heat Production: ~ 1.0 MMBTU/hr Other than coldest periods of winter, heat production exceeds demand Load Dump Radiator eliminates excess heat Fuel to Heat Efficiency 54% Overall Efficiency 86%

Power & Heat Production (+) Producing sufficient heat to satisfy demand of ESD and Lab Ops during coldest periods (-) Connected load is frequently not large enough to use all of the biogas being produced

Optimization Optimization of ESD Gas Production Balancing gas production with feeding times and quantities Maintaining cleansing velocity in line Look at potential co-feed feedstocks Storage Optimization of Power Production Not using all the biogas still flaring Add loads

Costs and Payback Elements of Capital Costs for Payback Analysis Gas Cleaning Skid Cogen Unit Hot Water Pumps for Cogen IEMS system PEX lines to Lab/Ops Total Additional Capital = $850,000

Estimated Savings Projected Energy Savings at Startup Rates $95,000/yr Projected Gas Savings at Startup Rates $47,000/yr Projected Payback 6 years simple, 7.8 discounted

Actual Savings Actual Energy Savings Approx $98,000/year Actual Gas Savings Approx $22,000/year Nat Gas is ½ price Utility bills have been lowered even with expanded plant! Approximately 25% of plant power is produced with CHP generator.

Where are we at today? Consistently producing between 170-200 kw power. Providing all heat necessary for digester and Lab/Ops. Balancing sludge feed rates to optimize gas production. Balancing heat draw from digester to better match production from cogen. Reviewing feasibility of another transfer switch.

Dial in Feed Rates Review and Optimize Load Usage vs. Energy Production Consider additional transfer switch Going Forward

Review Heat Usage vs. Production from Cogen Consider removing tubes from ESD HX Going Forward

Lessons Learned Micro-digestion Startup support Power Connection to Turbo-blowers Gas holder cover on old tank 3-way Valve Plug Coating Material vs. Temp Excessive Moisture in Bio-gas Improved primary efficiencies

Questions? Brian Hannon, P.E. Moore & Bruggink (616) 363-9801 bhannon@mbce.com Todd Wibright City of Grandville CWP (616) 457-0720 wibrightt@cityofgrandville.com