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A broader view to improve energy efficiency A project to improve a FCC unit s energy efficiency took into account surrounding process units to expand opportunities for saving energy and utilities NICOLAS LAMBERT and FILIPA GOUJARD Axens Greenhouse gas (GHG) emissions have become a growing concern for many industrialised countries over the past few years, as confirmed by the Paris Agreement in December 2015. Beyond the specific issues of GHG and general environmental considerations, there is a global tendency for improved energy efficiency. Indeed, whether the price of energy is high or low, controlled and reduced energy consumption will naturally improve operators margins. In the particular case of Russia, Presidential Executive Order number 752 was passed in September 2013, stating that the volume of GHG emissions will have to be reduced by 2020 to 75% of the baseline set in 1990. As indicated in the International Energy Agency s 2015 World Energy Outlook (Special Report on Energy and Climate Change), 1 Russia has indeed already drastically improved energy intensity between 1990 and 2014 (see Figure 1). Yet there is still a large potential for improvement in general and more particularly in the refining industry which represents about 5% of total energy use (including industry, transport and buildings). 1 This article will deal with the methodologies available to refiners to assess the thermal efficiency of their process, focusing on the case of the fluidised catalytic cracker (FCC) and its pre- and post-treatments, finally covering a revamp case of a refinery in the CIS area. Evaluating energy efficiency Pinch analysis is a systematic meth- Emissions, t / $1000 of GDP 2.4 2.0 China 1.6 India Russia 1.2 United 0.8 States Europe 0.4 Japan 0 0 3 6 9 12 15 18 21 CO 2 intensity, t/ capita odology for energy saving based on thermodynamic principles developed by Linnhoff March in the 1970s. It needs limited information about material (flow rate) and heat balance (temperature T, specific heat capacity Cp and enthalpy H). This method is useful to compare two networks, identify inefficient exchangers or assess the minimum energy (cold/hot utilities) required by the system, thus the maximum potential for improvement of a given scheme (the target). Pinch analysis never provides a solution but indicates routes to improvement. Moreover, this methodology cannot take into account specific process or operating constraints. As such, no optimised heat exchanger network (HEN) is obtained. Pinch analysis involves a graphical resolution through the building of composite curves. Composite curves aggregate, on an enthalpy/ temperature graph, all of the heat 1990 to 2014 Figure 1 Energy related CO 2 emissions per capita and CO 2 intensity by region. 1 Bubble area indicates total annual energy related CO 2 emissions. MER = market exchange rate availability in the process (the hot curve) on the one hand and all of the heat demands or heat sinks (the cold curve) on the other hand. The cold and hot composite curves therefore run more or less parallel. At the point where they are the closest to each other, the pinch temperature is defined and the difference in temperature at this point is called ΔT min (see Figure 2). With such a graphical representation, it is possible easily to identify design issues or poor exchanges. Indeed, thermal transfer will be impossible for instance if the cold curve is above the hot curve. In addition, three golden rules have been defined to ensure the best efficiency: No external cooling above the pinch No external heating below the pinch No heat transfer across the pinch. Properly integrated process units www.eptq.com PTQ Q2 2017 39

Temperature, ºC 350 300 250 200 150 100 Hot curve Cold curve 50 Cold utilities requirement 0 0 10 20 30 40 50 60 70 Power requirement, Gcal/h Figure 2 Example of composite curves routinely exhibit in the range 30-40 C. (This can vary depending on the process considered, site utilities conditions, and so on.) A target can be set with a lower, thus targeting a better efficiency. The cold composite curve is therefore translated until this new is reached. The new relative position of the cold and hot composite curves will then define the minimum hot and cold utilities consumptions necessary, and therefore the ultimate potential for energy savings. The optimum is a trade-off between investments (low ) and operating expenditures (high ), yet the pinch methodology will provide neither the optimum, nor the associated best possible optimised HEN. Pinch Hot utilities requirement Indeed, as previously indicated, pinch methodology provides only indications, for a given situation, that some exchanges are to be reviewed, not taking into consideration potential impossibilities due to technical limitations or process constraints. It is therefore necessary to use more sophisticated tools and this is why an in-house tool has been developed with IFP Energies nouvelles (IFPEN) in order to generate optimised HENs. This advanced tool needs much more data than pinch analysis and can be coupled directly with process simulators such as PRO/II. It is therefore possible to evaluate largescale units with added features: Bypass requirements can be set, in case the process needs to be run Figure 3 Previous maintenance work at the MNPZ FCC unit in Moscow Photo: Gazpromneft under different operating modes (seasonal operation, varying objectives of feed cocktail, for instance) or to take into account transient phases. Restrictions on approaches can be set. Some exchanges can be forbidden (high pressure fluid exchanging against low pressure fluid, very low duties, and so on). Number of exchanges can be limited to limit the complexity of the scheme (and associated capital expenditures). The target is generally defined as an energetic optimum but can be tweaked to take into account unit costs (opex), GHG regulations, minimum investment (capex), reduction in the consumption of a particularly expensive utility, or any combination of these. Consequently, the more data that is available, the larger the number of possibilities offered, and ultimately the better the HEN optimisation. This methodology has been applied to a FCC complex and the results are developed hereafter. The FCC complex Nowadays, a FCC unit can be thermally integrated to a large extent, especially when the unit is designed with a propylene recovery unit (PRU), which will allow good usage of low heat level streams to reboil columns such as a depropaniser and a deethaniser (see Figure 3). As such, it becomes fairly common to reach under 30 C while the industry standards are in general in the range 30-40 C. This seems to be the best performance achievable with conventional process equipment. Therefore, in order to get around such a limitation and seek even better performance, we have either to consider unconventional process or heat exchange equipment (generally available at a higher cost or with limited warranty due to reduced operational feedback) or expand the boundaries of the study. The latter will allow including more fluxes, thus a larger potential for further improved thermal integration as previously indicated. Therefore, instead of focusing 40 PTQ Q2 2017 www.eptq.com

only on the FCC unit, we shall have a look at the FCC complex. The FCC complex can for instance be defined as the chain of processes involving FCC feed hydrotreatment (cat feed hydrotreater, CFHT) and any or all of the post-treatments of the FCC effluents. Each element constituting this chain presents specific issues. In terms of flexibility: The FCC unit can be operated in different modes, resulting in fairly different yields, for instance maximum gasoline and maximum propylene modes of operation. The hydrotreating catalysts will age over time and exhibit different performances between start and end of run (SOR, EOR). Operating conditions can be tweaked to maintain optimal catalyst activity or adapted to the desired mode of operation, resulting in turn in different demands for utilities consumptions. Proper thermal integration should take into account those specifics and no compromise should be envisaged in order to ensure process integrity at all times and the requested level of flexibility intended for each process. The starting point for our case study is an FCC unit including a propylene recovery section for polymer grade propylene production with limited complexity with regards to energy efficiency. Moreover, in the chosen example: The pretreatment CFHT is operating in mild hydrocracking service, which increases middle distillate production through VGO hydroconversion while improving the quality of the VGO feeding the FCC unit. The post-treatment includes a gasoline hydrotreatment unit (GHT), in this case the Prime-G+ process enabling deep FCC gasoline desulphurisation with maximum octane retention. Two different thermal integration options have been considered for this chain of processes: Option 1 with deep thermal integration of each process separately, using pinch analysis and a linear programming tool Option 2 with thermal integration, allowing exchanges between process units. The balance between pre- Scheme Reference Option 1 Option 2 Optimisation Limited Independent units Global Complexity Low Normal Limited complexity Capex (MUSD) REF REF + 3% REF + 6% Opex (MUSD/yr) REF REF - 5% REF - 21% Pay back time (yr) - 2 1 complex 53 C 33 C 30 C FCC unit 25 C 16 C 16 C GHG (t eqco 2 /h) REF REF - 4.1% REF - 7.3% Table 1 and post-treatment was also slightly adjusted in order to maintain product qualities for a fair comparison. The exchanges have been limited in order not to jeopardise the operability of the units, including the possibility to start up and shut down properly. Moreover, neither breakthrough nor unconventional technologies have been envisaged. As expected, important gains were obtained versus the reference case. Some points in particular were noted (see Table 1): The FCC unit s efficiency for the reference case is already good but is further improved through an increase in the complexity of its heat exchanger network. While the FCC unit s efficiency seems to be the same (no variation in ΔT min between Phase 1 and Phase 2), the global thermal integration nevertheless also improved when exchange between the CFHT and the FCC/PRU was allowed. While the improvement in ΔT min Reduction, % 14 12 10 8 6 4 2 0 Case study around the FCC complex Systematic application could seem marginal, whether looking at the FCC unit alone or the whole complex, large gains were obtained in terms of opex or GHG emissions for a limited increase in complexity and capex (limited number of additional process/process exchanges). It appears that tracking ΔT min alone will not allow full assessment of the performance of a scheme, as variations in ΔT min do not directly reflect variations in reduction of opex, GHG emissions or specific utility consumption. As such, setting clear objectives is of paramount importance to ensure that the best scheme will be offered. Obviously, resorting to nonconventional technologies, while certainly more expensive to install or more complex to operate, will further boost the energy efficiency of such a complex. We can name, in decreasing order of contribution to the reduction of GHG emissions (see Figure 4): Integration unit-by-unit Good integration Hydraulic power recovery turbine Divided wall column Side reboilers Case-by-case analysis Advanced heat exchangers Organic Rankine cycle (theoretical) Figure 4 Further reduction of GHG emissions with non-conventional solutions www.eptq.com PTQ Q2 2017 43

Temperature, ºC 40 30 20 10 0 0 25 50 75 100 125 150 175 200 Duty, Gcal Figure 5 Pinch analysis of the existing units Organic Rankine cycle (ORC), consisting of heat recovery from a lower temperature converted into useful work that could itself be converted into electricity thanks to an expansion device such as an expander. Dividing wall columns, their optimal application being limited to spare applications in the FCC complex. Indeed, all fractionation services are not suitable for such technology. Use of side reboilers: this is limited to a handful of applications for minor gains throughout the FCC complex. Advanced heat exchangers: use of advanced technologies will be envisaged only in specific cases (for instance, a retrofit where plot space or pressure drop are issues). Hydraulic power recovery turbines can be considered whenever a high pressure to low pressure letdown is considered. All of the above will contribute separately to GHG emissions reduction above and beyond the intra- or inter-thermal integrations. A better level of performance from these solutions is expected, as more and more operators will resort to their use. CFHT and FCC unit revamp case in the Gazpromneft Moscow Oil refinery (MNPZ) Axens recently managed a revamp case in the MNPZ refinery. This consisted of debottlenecking the capacity of a train composed of a CFHT and FCC unit, along with better performance and improved energy efficiency. As part of the FCC Alliance, Axens and its partner TechnipFMC have a track record of successful FCC grassroot designs and revamps. This project went through different steps, under initial management by Performance Programs, Axens unit in charge of consulting services, 2 in order to ensure proper execution and fulfilment of Gazpromneft s expectations at the lowest possible cost: A feasibility study, consisting of: Identification of main bottlenecks Proposing incremental capacity increases vs cost Selection of the (economically) optimum capacity for the complex (CFHT+FCC unit) A scoping study with a higher level of precision: Focusing on a selected case (capex/opex) Confirmation of the profitability of the case Full site survey and thermal integration study aiming at identifying one preferred scheme, taking into account process and site constraints Process data book production. Beyond the expected improvement in energy efficiency and increase in capacity, a technological upgrade was performed on the FCC unit involving, among others: the installation of new impact-type feed injectors to ensure intimate contacting of feed molecules with catalyst particles; replacement of the riser termination device with RS² in order to limit dry gas production due to thermal degradation of the products; and addition of new stripper packing for enhanced recovery of hydrocarbons. Concerning the CFHT operating in mild hydrocracking service, a new reactor distribution tray was installed using EquiFlow technology. Moreover, a new fractionator aiming at removing diesel from the FCC feed was added to the plant. A preliminary pinch evaluation of the existing configuration hinted at different potential improvements. Indeed, the ΔT min at 68 C was probably too high with regard to current industry standards and different breaches of the aforementioned golden rules were also identified (see Figure 5): Seven exchanges across the pinch Eight exchanges with cold utility above the pinch One exchange with hot utility below the pinch. Further to the pinch analysis, in-house HEN optimisation software was used to produce different solutions: Case 1: no constraints provided. This case was set to allow the ultimate potential gains possible to be defined for benchmarking the other cases. Case 2: process/process exchanges allowed only for duties higher than 0.5 Gcal/h. This case targeted limiting overall capital expenditures yet resulted in achieving about twothirds of the maximum potential reduction in energy consumption. Case 3: full flexibility to account for transient phases and refiner s preferences. For instance, exchanges between high and low pressure fluids were banned, as well as exchanges between CFHT recycle gas and any FCC unit streams. In addition, a minimum bypass of 10% was requested in order to maintain unit controllability. Obviously, each demand aiming at increased operational safety/reliability, or reducing operational complexity, would be made at the expense of the final energetic performance of the process units. Case 3 was retained as the 44 PTQ Q2 2017 www.eptq.com

Main fractionator Top HCO Slurry Figure 6 New arrangement around FCC fractionator Among these modifications, we can in particular detail rearrangebasis for further steps, in spite of preliminary moderate improvement in energy requirements (about onethird of the maximum potential reduction in energy consumption), as this was a very realistic basis with a reduced number of modifications, above all in line with the refiner s budget. After careful examination of the units performances and behaviour through a site survey and checkrun, the thermal integration study was finalised and data sheets produced. The following modifications in the heat exchange equipment were performed: DeC3 Reboiling VGO HDT reactor feed Preheat VGO HDT fractionator feed Preheat CFHT CFHT FCC FCC Complex Complex (old) (new) (old) (new) (old) (new) CW consumption, Gcal/h 0.2 3.7 26.5 22.1 26.7 25.8 FG consumption, Gcal/h 25.3 19.4 - - 25.3 19.4 Added steam production, Gcal/h - 8.0 - - - 8.0 Throughput, T/h 254 300 246 275 254 300 Efficiency, Gcal/T feed 0.10 0.05 (-50%) 0.11 0.08 (-27%) 0.21 0.12 (-43%) opex, $million/y 3.3 Table 2 Energy efficiency improvement in MNPZ refinery CFHT One fired heater modified One air cooler deleted Six new heat exchangers and two new air coolers corresponding to the addition of a fractionator aimed at removing diesel from the FCC feed. FCC One heat exchanger removed Two air coolers and two exchangers replaced for larger capacity Three reboilers modified to improve performance. Before revamp After revamp Delta CFHT flow rate 254 T/h 300 T/h +18% FCC flow rate 246 T/h 275 T/h +12% Catalyst cycle length 2 years 2 years - Extra diesel production flow rate 0 19 T/h +19 T/h Gasoline production 130 T/h 162 T/h +25% LCO production 27 T/h 23 T/h -15% Utilities consumption (Gcal/t feed) 0.21 0.12-43% Table 3 Global improvements of MNPZ CFHT and FCC unit ments around the FCC unit s main fractionator column (see Figure 6): The depropaniser is now reboiled with top pumparound) instead of HCO pumparound The subsequent heat available in HCO pumparound is now used to preheat CFHT feed instead of using slurry pumparound The subsequent heat available in slurry pumparound is now used to preheat new CFHT fractionator feed. Finally, results were obtained where utilities consumptions have been averaged between summer and winter operations in order to account for seasonal variations of air/water cooling breakpoint (see Table 2). Added electrical consumption by rotating machines was not taken into account to focus on improvement of energy efficiency rather than on capacity increase. Added electrical consumption by air coolers was considered negligible. The total revamp investment for capacity increase, technology upgrade and thermal efficiency is $52.8 million. Looking only at air cooler and heat exchanger investments (not pertaining only to energy efficiency), this corresponds to $13.5 million, thus a payback time of four years in spite of a significant capacity increase. The global impact of the revamp is detailed in Table 3. All of the objectives set for Axens were met with outstanding improvement in energy efficiency for a limited added level of complexity, without impacting the operability of the unit or the CFHT cycle length in spite of strong constraints imposed due to plot plan limitations. Conclusion The growing scarcity of resources, climate change and growing populations on the one hand and a fluctuating market with tightened refining margins on the other hand are defining a new context imposing more energy efficient plants. Considering only pinch ΔT as an indicator for process unit efficiency is not sufficient to compare solutions; taking into account objec- 46 PTQ Q2 2017 www.eptq.com

tives and site specifics is paramount and imposes a tailor-made solution. Such a solution must not impair the reliability or the flexibility of the processes involved to cope with varying feedstocks and evolving process objectives. Moreover, ensuring operability on a daily basis is crucial. Broadening the vision around main process units such as the FCC unit to include surrounding process units will offer better opportunities for improvement in global energy efficiency, whether non-conventional solutions are considered or not. As such, management of the FCC train for instance by a single licensor can help to reduce drastically GHG emissions and/or utilities consumptions. As illustrated in this article, Axens is developing a sustainable approach that minimises environmental footprints through tailor-made solutions. The company s experience as a technology licensor shows that, due to tight schedule and lack of time, energy efficiency and water footprint are not sufficiently customised and this can be improved with an approach called Custom and Efficient Early Design (CEED). During this new phase, taking place before the beginning of basic engineering, Axens and the operator work in close collaboration. In addition to the base case, alternate schemes are defined and carefully evaluated according to several criteria defined by the operator (capex, opex, IRR, NPV, energy efficiency, water footprint, unit flexibility, unit operability and so on). At the end of the CEED phase, Axens provides a decision support tool that enables the operator to select the most appropriate scheme for the basic engineering phase. As a technology licensor, Axens ensures that the proposed optimal scheme is robust and safe, considering all the flexibility needs such as various operating modes, start-up needs and specific catalyst treatment steps. Therefore additional scrutiny by another layer of experts is not warranted, potentially saving significant cost and schedule impacts. References 1 International Energy Agency, World Energy Outlook 2015, Special Report on Energy and Climate Change. 2 Axens Consulting Performance Programs, www.axens.net/our-offer/ by-products/services/consulting-performance-programs.html Filipa Goujard is a Project Engineer within the Consultancy and Project Group, Performance Programs Business Unit of Axens, particularly involved in energy efficiency audits. She previously worked as a Process Engineer and R&D Project Manager in the field of catalysis and holds a PhD in industrial, organic and mineral chemistry from the University of Poitiers, France. Nicolas Lambert is Technologist in the Middle Distillates and Conversion Business Line, Axens Process Licensing Business Unit, in particular in charge of FCC technologies. He joined Axens as a Process Engineer and successively served as Project Manager for aromatics, reforming and FCC technologies. He is an engineering graduate from Arts & Métiers ParisTech (ENSAM). www.eptq.com PTQ Q2 2017 47