Selective Use of Oxygen and In- Furnace Combustion Techniques for NO x Reduction in Coal Burning Cyclone TM Boilers

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Technical Paper BR-1809 Selective Use of Oxygen and In- Furnace Combustion Techniques for NO x Reduction in Coal Burning Cyclone TM Boilers Authors: H. Sarv A.N. Sayre G.J. Maringo Babcock & Wilcox Power Generation Group, Inc. Barberton, Ohio, U.S.A. R. Varagani S. Levesque American Air Liquide Newark, Delaware, U.S.A. Presented to: 33rd International Technical Conference on Coal Utilization & Fuel Systems Date: June 1-5, 2008 Location: Clearwater, Florida, U.S.A.

Selective Use of Oxygen and In-Furnace Combustion Techniques for NO x Reduction in Coal Burning Cyclone TM Boilers H. Sarv, A.N. Sayre and G.J. Maringo Babcock & Wilcox Power Generation Group, Inc. Barberton, Ohio, U.S.A. R. Varagani and S. Levesque Air Liquide Newark, Delaware, U.S.A. Presented at: 33rd International Technical Conference on Coal Utilization & Fuel Systems Clearwater, Florida, U.S.A. June 1-5, 2008 BR-1809 Abstract A nitrogen oxides (NO x ) minimization strategy for coalburning Cyclone TM boilers was developed that includes deep air staging, innovative oxygen use, reburning, and advanced combustion control enhancements. Computational fluid dynamics modeling was applied to refine and select the best arrangements. Pilot-scale tests were conducted by firing an eastern high-volatile bituminous Pittsburgh #8 coal at 5 million Btu/hr in a facility that was setup with bi-level overfire air ports. Oxygen enrichment of the Cyclone combustor enabled high-temperature and deeply staged operation while maintaining good slag tapping. Firing the Pittsburgh #8 coal in the optimum arrangement generated 112 ppmv NO x (0.15 lb/million Btu) and 59 ppmv CO. The optimum emissions results represent 88% NO x reduction from the uncontrolled operation. Introduction Coal-burning Cyclone boilers in the U.S. account for approximately 26,000 MW of electric generation capacity. Cyclone-equipped furnaces were originally developed to burn a wide range of crushed coals with low fly ash handling expenses and fuel preparation costs. Due to the intense turbulent mixing of coal and air, and the high-temperature combustion, NO x (NO+NO 2 ) emissions from Cyclone furnaces typically exceed 1.2 lb/10 6 Btu, requiring staging, fuel reburning, and/or backend pollutant control technologies for compliance with environmental regulations. Current commercial performance for eastern bituminous coal combustion in air-staged Cyclone units has been around 0.5 to 0.6 lb NOx/10 6 Btu. Fuel reburning is another proven technology for NO x reduction in Cyclone boilers. In the conventional coal reburning, baseline NO x levels drop by 40 to 60% when 20 to 30% of the heat is released by the supplementary fuel downstream of the main combustion zone. 1 Selective use of oxygen in the combustion zone can extend the sub-stoichiometric operating range and offer the potential for lowering the NO x emissions relative to other infurnace NO x control methods. Under the joint sponsorship of DOE-NETL, Babcock & Wilcox (B&W) Power Generation Group, Inc. and Air Liquide, a program was undertaken for minimizing the NO x emissions in coal-burning units including those equipped with Cyclone furnaces. Our NO x reduction approach for coal-burning Cyclone boilers was based on sub-stoichiometric operation of the main combustion zone, deeply staged reburn zone, and managed use of oxygen and recycled flue gas in selective combustion zones. Modeling simulations Prior to pilot-scale testing, a range of operating parameters (e.g., Cyclone stoichiometry, extent of reburning, pure O 2 distribution and dispersion, flue gas recycle flow, etc.) were simulated with the aid of the B&W combustion model COMO SM. COMO is a multi-dimensional computational fluid dynamics code with advanced capabilities for simulating turbulent flow, particle trajectories, heat transfer, radiation, and heterogeneous and gas-phase reactions. It uses an unstructured mesh with a mixture of element shapes, and adaptive mesh refinement for higher resolution in regions of high temperature, velocity, or concentration gradients. COMO simulated the furnace, Cyclone combustor, reburn burners, overfire air ports, and oxygen injectors with sufficient control volumes. Figure 1 shows the computer model of the Cyclone combustor. Computer simulations included Babcock & Wilcox Power Generation Group 1

Fig. 1 Computer model of the Cyclone TM combustor. sub-stoichiometric combustion of a high-volatile Pittsburgh #8 coal in the Cyclone furnace at part load operation (70% firing rate in Cyclone combustor and 30% in reburn burners) with and without oxygen enrichment, and the baseline full load (100% firing rate in Cyclone combustor) air-blown operation without oxygen addition. Figure 2 compares the predicted temperature and oxygen concentration contours of three cases representing sub-stoichiometric Cyclone operation. Without oxygen enrichment, the Cyclone furnace was cooler at 70% firing rate (middle left plot) in comparison with 100% firing operation (lower left plot). Oxygen enrichment in the Cyclone furnace at the 70% firing rate had a similar temperature profile (upper left plot) to 100% firing rate without oxygen enrichment (lower left plot). Here, oxygen enrichment is the equivalent percentage of pure O 2 flow divided by the total oxygen that flows into the boiler by various oxidant streams (i.e., air, pure O 2, and the recycled flue gas). Point sources of locally high O 2 concentrations are also evident at the secondary air inlet to the Cyclone where oxygen was injected via a multi-hole lance (upper right plot). Predicted O 2 profiles on the right hand side of Figure 2 indicate rapid consumption of the pure oxygen stream under sub-stoichiometric Cyclone conditions. Since hot and oxygen-deficient combustion zones are conducive to nitric oxide destruction, oxygen injectors and reburn burner design selections for testing were based on these attributes, and thus NO x was not predicted. Pilot-scale facility description Pilot-scale tests were performed in B&W s Small Boiler Simulator (SBS) facility, located in Alliance, Ohio. The water-cooled SBS furnace measures 4.5 ft wide by 7 ft deep by 17 ft high. The inside surface of the SBS furnace is insulated to yield a furnace exit gas temperature of 2100F or higher when firing a high-volatile bituminous coal at full load. Figure 3 illustrates the Cyclone firing configuration of the SBS. A calibrated gravimetric feeder controls the coal flow to the Cyclone. For aerodynamic similarity, coarse pulverized coal instead of crushed coal (which is typical in commercial units) is carried by heated primary air in the transport pipeline and into a scroll burner on one end of the Cyclone. Tertiary air is introduced from the center of the scroll burner to control the position of the main flame in the Cyclone. As the coal/air mixture enters the Cyclone barrel, it encounters a high-speed vortex from the 800F secondary oxidant. Both the primary and secondary air streams swirl in the same direction. Fine coal particles burn in suspension and exit the center cone with hot gases. Due to the centrifugal action, large particles are captured and burned in a molten layer of slag that forms on the inner walls of the Cyclone. The molten mineral matter exits the Cyclone furnace from a tap below the Cyclone throat and drops into a water-filled slag tank. About 80% of the coal ash leaves the Cyclone as slag. For staged combustion, the Cyclone furnace was operated sub-stoichiometrically to minimize the NO x formation. Staging air was introduced at two elevations each equipped with two overfire air (OFA) ports. Damper control and pressure drop indicators across the in-duct orifice plates were used to balance the airflow to each OFA port. In the reburning arrangement, two single-register burners fired pulverized coal above the main combustion zone. For maximum operational flexibility, the reburn burner design featured a retractable central coal nozzle, a surrounding annulus with moveable spin vanes for swirling the flue gas recycle (FGR) flow, and a retractable oxygen lance. Reburn coal was supplied and controlled by a calibrated screw feeder, transported by unheated primary air, and split equally between two reburn burners. Combustion products exited the furnace and entered a convection tube bank. Stack gases were sampled continuously from the convection pass section outlet through a heated sample line. Gas sampling was done at about 700 to 800F. After filtering and drying, CO, CO 2, O 2, SO 2, and NO x concentrations were measured by calibrated analyzers. Oxygen concentration of the secondary oxidant stream to the Cyclone furnace was measured by fast-response, in-situ O 2 sensors. Fly ash was sampled across the convection pass section exit via an isokinetic probe. Non-intrusive flame imaging and temperature mapping were done with a two-color optical pyrometry system called FLAMEVIEW TM. The unit comprises a CCD (Charge Coupled Device) camera mounted on the roof of the SBS. Two-dimensional temperature maps were generated by processing the flame signal in the visible and near infrared regions. Liquid oxygen was delivered by trucks and stored in a 9,000-gallon tank. The liquid oxygen was vaporized in an ambient vaporizer. Gaseous oxygen was then regulated to appropriate pressures for delivery to the test area. Existing PLC (programmable logic controller) and HMI (humanmachine interface) systems were upgraded and integrated into the SBS safety interlocks, allowing oxygen flows to be safely and accurately controlled and monitored from a cen- 2 Babcock & Wilcox Power Generation Group

Fig. 2 Computed mid-plane countour plots of temperature (K) and O 2 (mole fraction) for staged combustion of Pittsburgh #8 coal in the Cyclone furnace at 0.80 stoichiometry. tral valve skid to various combustion zones. Figure 4 shows a multi-hole lance for injecting oxygen into the secondary air inlet of the Cyclone furnace. Test results A high-volatile, eastern bituminous Pittsburgh #8 coal was used for testing. Table 1 lists the proximate, ultimate, and heating value of the as-received coal sample. Ash composition is listed in Table 2. Pulverizer settings were adjusted to produce the desired fineness. Pulverized coal samples were checked for fineness using stacked sieves of 200 to 30 mesh screens (74 to 595 μm). Table 3 tabulates two as-fired pulverized coal finenesses for the reburn burners. Baseline performance data were collected without oxygen enrichment or reburning. Optimum secondary air damper Babcock & Wilcox Power Generation Group 3

Fig. 3 Cyclone-fired configuration of small boiler simulator. settings for steady slag tapping and minimum pollutant emissions (NO x, CO) were determined at full load (5 x 10 6 Btu/hr) and 3.2% O 2 at furnace exit (corresponding to 1.17 overall stoichiometry, or 17% excess air in the air-blown case). Soot formation tendency for Pittsburgh #8 coal was generally strong and it increased as the combustion stoichiometry was lowered. At high combustion temperatures soot particle radiation gave the luminous flame appearance. Birdseye view flame images and 2-D temperature maps of the Cyclone combustor exit are shown in Figure 5. Flame luminosity and combustion temperature peaked at stoichiometric operation (SR=1.0) but decreased at 0.85 and 1.17 stoichiometries. Optical viewing of the Cyclone exit zone became more challenging at 0.70 combustion stoichiometry due to the dimming effects of lower combustion temperature and obscuration by soot. Depending on the Cyclone combustor stoichiometry and OFA distribution, the NO x levels ranged from 0.2 to 1.4 lb NO x /million Btu as shown in Figure 6. NO x emissions were lower when the staging air was split equally between the rear (lower) and front (upper) OFA ports. Single level OFA ports provide good air jet penetration and mixing with the flue gas stream but they also cause the oxidation of nitrogen-carrying species that form under deep Multi-hole oxygen lance Fig. 4 Oxygen enrichment Figure 4. Oxygen enrichment in the Cyclone in the cyclone furnace. staging. Bi-level staging of air can be more effective for NO x minimization than single-level because the gradual addition of OFA above the combustion zone reduces the oxidation of nitrogenous species. When all of the staging air was blown through the upper OFA ports, the unburned combustibles also increased due to gas temperature cooling in the upper furnace. Figure 7 provides further verification that equal distribution of the OFA at two levels was more effective than single-level operation with or without any coal reburn. Figures 8 and 9 show the effect of FGR addition to the Cyclone furnace on NO x and CO emissions under unstaged 4 Babcock & Wilcox Power Generation Group

Fig. 5 Flame images and 2-D temperature maps of the Cyclone combustor exit obtained by the FLAMEVIEW TM optical pyrometry system while burning Pittsburgh #8 coal at different stoichiometric ratios (SR). Flow direction is from left to right. and staged conditions. In the unstaged mode and with 19% flue gas recycle, the volumetric O 2 concentration in the secondary oxidant stream to the Cyclone furnace dropped from 20.8% to 17.5% (on a wet basis) resulting in 11% lower NO x emissions relative to no recycle operation. Thermal quenching and lower oxygen partial pressure are the most likely reasons for the observed NO x suppression. Recycling of 13.5% flue gas into the staged Cyclone lowered the secondary oxidant stream O 2 concentration from 20.8% to 16.9%. But due to its cooling effect on the sub-stoichiometric NO x destruction zone, the NO x emissions increased by 5%. In both cases (staged and unstaged) CO emissions increased only slightly and slag tapping was not noticeably affected by flue gas recirculation. Coal reburning of up to 27% of the total fuel input was done downstream of the staged Cyclone combustor (0.70 stoichiometry with bi-level OFA addition). Despite the already reducing conditions of the main combustion zone, coal reburning was able to further trim the NO x emissions to their lowest values in the 9-18% coal reburn range as shown in Figure 10. Within this range, the combined Cy- clone furnace and reburn burner stoichiometry in the reburn zone was 0.63 to 0.68. At 27% coal reburn, the reburn zone stoichiometry dropped slightly below 0.60 and some of the evolving nitrogenous species were oxidized by the overfire air to NO x. Utilization of a coarser reburn PC (73% versus 90% through a 200 mesh screen) under the air-blown mode of operation had a negligible effect on NO x emissions but it elevated the unburned combustibles by 5% due to incomplete burnout of larger particles. Oxygen enrichment of the staged Cyclone furnace was evaluated by partial substitution of air with O 2. Various O 2 lances were installed sequentially through the scroll burner and the secondary air entrance to the Cyclone barrel. Consistent with the computer modeling predictions, oxygen enrichment by way of a multi-hole lance at the secondary air inlet to the Cyclone barrel was more effective than the centerline scroll burner lance. Without coal reburn, oxygen enrichment of the staged Cyclone furnace (SR=0.7) at 2 to 10% of the total O 2 flow into the boiler resulted in 0.17 to 0.18 lb NO x /10 6 Btu. With 10% coal reburn and 5 to 7% oxygen enrichment, the NO x levels were 0.15 lb/10 6 Btu or Fig. 6 Cyclone combustor stoichiometry and OFA distribution effects on NO x emissions from the combustion of Pittsburgh #8 coal. Nominal operating conditions: 5 MBtu/hr and 1.17 overall stoichiometry. Fig. 7 Bi-level OFA distribution effect on NO x emissions for staged combustion of Pittsburgh #8 coal with and without reburning at 5 MBtu/hr, 0.70 Cyclone combustor stoichiometry, and 1.17 overall stoichiometry. Babcock & Wilcox Power Generation Group 5

Fig. 8 Effect of flue gas recycle into the Cyclone combustor on NO x and CO emissions during unstaged operation with Pittsburgh #8 coal at 1.17 stoichiometry and 5 MBtu/hr. lower as shown in Figure 11. In both cases, the unburned combustibles remained unchanged over the entire range of pure O 2 flow to the Cyclone furnace. Without oxygen enrichment, the minimum stoichiometry to avoid slag buildup and plugging in the Cyclone throat was 0.7. Adding 10% oxygen to the Cyclone furnace enabled high-temperature and deep-staged operation at 0.6 stoichiometry. Optimum Cyclone firing performance results at 5 million Btu/hr firing rate and 1.17 overall stoichiometry for the staged combustion of Pittsburgh #8 coal using bi-level OFA configuration, with and without oxygen enrichment or coal reburn are summarized in Figure 12. Best performance results of 111 to 112 ppmv NO x (0.146 to 0.150 lb/million Btu), 59 ppmv CO, and good slag tapping from the bottom of the primary furnace were achieved at 0.70 Cyclone combustor stoichiometry, 10% coal reburning, and with O 2 enrichment at only 5 to 7% of the total equivalent oxygen flow to the boiler. These optimum emissions results represent 88% NO x reduction from the uncontrolled operation. Fig. 10 Extent of coal reburning effect on NO x emissions from the combustion of Pittsburgh #8 coal. Nominal operating conditions: 5 MBtu/hr, 0.70 Cyclone stoichiometry, 17% overall excess air, and reburn coal fineness of 90% through a 200 mesh screen. Fig. 11 O 2 enrichment effects on NO x emissions from the combustion of Pittsburgh #8 coal in the Cyclone furnace. Nominal operating conditions: 5 MBtu/hr, 0.70 Cyclone stoichiometry, 1.17 overall stoichiometry, and 10% reburn with 73% fineness through a 200 mesh screen. Fig. 9 Effect of flue gas recycle into the Cyclone combustor on NO x and CO emissions during staged operation with Pittsburgh #8 coal at 0.75 stoichiometry using lower level OFA ports. Nominal operating conditions: 5 MBtu/hr and 1.17 overall stoichiometry. Fig. 12 Firing configuration and operating condition effects on NO x emissions from burning Pittsburgh #8 coal at 5 MBtu/hr, 0.70 Cyclone furnace stoichiometry, and 1.17 overall stoichiometry. 6 Babcock & Wilcox Power Generation Group

Acknowledgments This paper is based upon work supported by the U.S. Department of Energy under Award Number DE-FC26-05NT42301. The project was funded by the US Department of Energy - National Energy Technology Laboratory s (DOE-NETL) Innovations for Existing Plants Program. The authors would like to thank the DOE Project Officer, Bruce Lani for providing insightful advice during the course of the program. Assistance of Terry Wilson, Larry Mohr, Jeff Dudley, Vern Burch, Robby Porter, Mike Shea, Charlie Stauffer, Bartev Sakadjian, and Lisa Rimpf in the pilot facility operation and instrument calibration is also greatly appreciated. References 1. Farzan, H., Wessel, R.A., Sarv, H., Kim, R.K., Rodgers, L.W., Maringo, G., and Yagiela, A.S., Reburning Scale-up Methodology for NO x Control in Cyclone Boilers, Presented at the ASME International Power Generation Conference, Paper No. 91-JPGC-FACT-13, San Diego, CA, October 1991. Copyright 2008 by Babcock & Wilcox Power Generation Group, Inc. a Babcock & Wilcox company All rights reserved. No part of this work may be published, translated or reproduced in any form or by any means, or incorporated into any information retrieval system, without the written permission of the copyright holder. Permission requests should be addressed to: Marketing Communications, The Babcock & Wilcox Company, P.O. Box 351, Barberton, Ohio, U.S.A. 44203-0351. Or, contact us from our Web site at www.babcock.com. Disclaimer Although the information presented in this work is believed to be reliable, this work is published with the understanding that The Babcock & Wilcox Company and the authors are supplying general information and are not attempting to render or provide engineering or professional services. Neither The Babcock & Wilcox Company nor any of its employees make any warranty, guarantee, or representation, whether expressed or implied, with respect to the accuracy, completeness or usefulness of any information, product, process or apparatus discussed in this work; and neither The Babcock & Wilcox Company nor any of its employees shall be liable for any losses or damages with respect to or resulting from the use of, or the inability to use, any information, product, process or apparatus discussed in this work.