SCR Retrofit Improves Performance

Similar documents
Controlling NOx and other Engine Emissions

Coal Pipe Coal Flow Distribution Control for Coal Pulverizer Systems

natcom burner solutions Advanced burner technology for stringent emissions requirements

SCR RETROFIT FOR NO X REDUCTION EXPERIENCES IN CHINA & POLAND TWO COUNTRIES WITH COAL AS DOMINATING FUEL SOURCE

Honeywell UOP Callidus Solutions

SCR and Zero-Slip TM Technology

MONTHLY TECHNICAL PROGRESS REPORT. Product Design Improvement

TECHNICAL PUBLICATION

Optimizing Spray Performance with Computational Fluid Dynamics. From Spraying Systems Co. Spray Analysis. Spray Control.

Peerless Europe. Separation and Filtration

Reflux Samplers for Process Gas Chromatographs Their Use and The Importance of Product Design

GE solutions for NOx compliance and increased availability for WtE / Biomass plants

PureCycle 200 Heat-to-Electricity Power System

BAG FILTERS (BAGHOUSES)

CALL FOR COMBINED HEAT AND POWER (CHP) PROJECTS. Program Guide

Productivity versus Profitability in Vacuum Web Coating

Development of Phosphoric Acid Fuel Cell Stack

Integrated CHP Using Ultra-Low-NOx Supplemental Firing

CPS Creative Power Solutions

Feasibility study of a roof top Solar room heater

Potentials and Limitations with respect to NO x -Reduction of Coke Plants

High efficient peak power on demand. Answers for energy.

Kalex Kalina Cycle Power Systems For Use as a Bottoming Cycle for Combined Cycle Applications

Thermal Mass Flow Meters Help Reduce Energy Costs and Enhance Emissions Monitoring Systems

Controlling Ammonia-in-Ash through Direct Measurement of Ammonium Bisulfate

Operational flexibility enhancements of combined cycle power plants

Plant construction and waste heat systems for the chemical industry

COMBINED CYCLE OPPORTUNITIES FOR SMALL GAS TURBINES

Renovating a Medical Radiosotope Production Hot Cell T. GROCHOWSKI ROBATEL Technologies

TruePeak TDLS200. NH 3 Slip Measurement. <Document Number> Copyright Yokogawa Electric Corporation <date/time>

FlexEfficiency* 60 Portfolio

System Assessment Capabilities for Nuclear Power Stations

DEVELOPMENT AND USE OF SIMULATION TRAINERS FOR PIPELINE CONTROLLERS. D.M. Scott Enbridge Pipe Line Company Edmonton, Alberta, Canada

COMBUSTION OPTIMIZATION OF A 150 MW (NET) BOILER UTILIZING AIR AND FUEL FLOW MEASUREMENT AND CONTROL

Catalytic Activated Ceramic Dust Filter a new technology for combined removal of dust, NOx, dioxin, VOCs and acids from off gases.

GUIDE SPECIFICATIONS CURA ADJUSTABLE REROOF FRAMING SYSTEMS SECTION REROOFING ADJUSTABLE FRAMING SYSTEM

Biomass Boiler Emission Abatement Technologies. Simon Wakefield

Ovivo Carrousel Systems

IDENTIFICATION OF VENTILATION PROBLEMS IN AN UNDERGROUND BUS TERMINAL IN KOREA

Understand boiler performance characteristics. Use these suggestions when buying, designing or optimizing steam generators

High Bridge Combined Cycle Plant

Fluid Mechanics, Heat Transfer, Thermodynamics. Design Project. Production of Ammonia

Outreach Report Water Wall Turbine Inc.

TEMPERATURE AND HEAT DISTRIBUTION PROTOCOL FOR PROCESSING IN DISCONTINUOUS AGITATING RETORTS

Turbine Tip Clearance Issues and Optimization for Increased Power and Efficiency. Lloyd Cooke Liburdi Turbine Services Inc

97 MW of Cat coal seam methane power in New South Wales, Australia

RECENT DEVELOPMENTS IN ANODE BAKING FURNACE DESIGN

Furnaces for Research and Laboratory. Testing Drying Ashing Tempering Preheating Sintering Firing Annealing

Electric Furnace Off-Gas Cleaning Systems Installation at PT Inco ABSTRACT

Fossil Materials and Repair - Program 87

Basic design of laboratory bioreactor

NTPC O&M Conference Performance and Optimization of Water Utilisation Increase of Existing Power Plants. Speaker Name; Tufani Ram 13-14/02/2013

Effect of Rotation Speed of a Rotary Thermal Wheel on Ventilation Supply Rates of Wind Tower System

Underf loor For Schools

PPC specializes in maximum efficiency air pollution control equipment using a variety of different

REQUEST FOR QUALIFICATIONS. Design/Build Project Number CP Power Plant - Boiler 10 Gas Burner Replacement

Company brochure. turbotect турботект

WASTE HEAT BOILERS FOR NITRIC ACID, CAPROLACTAM AND FORMALDEHYDE PLANTS

COOLING EFFECT ENHANCEMENT IN MAGNETRON SPUTTERING SYSTEM

Valbart Through Conduit Slab Gate Valve (TCSGV)

Automation System Optimization

THE POWER TO DO MORE. Cat Gas Generator Sets

Post Combustion CO 2 Capture Scale Up Study

Pneumatic Mortar Development for the NASA/Orion Capsule Drogue Parachute System

RTO OR RCO FOR VOC CONTROL: HOW TO DECIDE

California Chrome Shop Masters Tough Regulations James Bauer Manufacturing Engineering Manager Robbins & Myers, Inc. Fairfield, California

COMPLETE REVISION April Process Industry Practices Piping. PIP PNC00004 Piping Stress Analysis Criteria for ASME B31.

MonTech RP 3000 Rapid Plastimeter for Polymers and Natural Rubber

WELLHEAD POWER PLANTS

Static Mixing, Reaction, Heat Transfer & Fluid Dynamics Technology

Aqua-Swirl Stormwater Treatment System

Diode laser analyser LS4000 Ammonia slip measurement for DeNOx process

Reducing Harmful Emissions Discharged into the Atmosphere from Operating Boilers by Applying a Combination of Low-Cost Technological Measures

HRSGs, Waste Heat Boilers & Aftermarket Services

Tailor-made SNCR to Meet Future Emission Standards for Power Boilers

Intelligent Process Cooling Technology Saves on Water and Energy, Improves Productivity

Topsoe s Emission Management Solution--DeNOx

5.2 MW Solar Mobile Power Unit

Determining SCR Reactor Potential In situ Paper # 17

Swansea Bay tidal powerplant: Bi-directional bulb pump-turbine with variable speed

Orlando Utilities Commission

Retrofit of Rodenhuize 4 power station: The Max Green and Cold Back-up-projects

DESIGN BASIS FOR AIR CONDITIONING AND VENTILATION SYSTEM FOR SUBSTATION AND CONTROL BUILDING HINDUSTAN PETROLEUM CORPORATION LTD.

Product Inspection. Compliance Expertise Performance Uptime. Product Inspection Services Maximizing Productivity

Ten Year Retrospective Look at HRSG FAC Assessment and Incidence. Peter S. Jackson, PhD, PE, David S. Moelling, PE, Mark Taylor, Mech. Eng.

THE STUDY OF THE BAKING OVENS BY COMPUTER SIMULATION

ABS Software Brochure

HRSG Inspection Tasks. HRSG Inspection

Fluid Mechanics, Heat Transfer, Fluid Mechanics Design Project. Production of Ethanol

Thermal advantages for your production line Thermal Solutions

Operating Status of Uprating Gas Turbines and Future Trend of Gas Turbine Development

Induced Gas Flotation (IGF) within an API Skim Tank A Case Study of Design Approach and Results

Functional FOLDS BY JONATHAN L. BAYREUTHER, PE, AND JONATHAN HAMANN

Specifying metal studs for interior and exterior walls can be simple.

CLCF Climate Changer for comfort applications. Next generation air handling performance from Trane

ANSYS Combustion Analysis Solutions - Overview and Update

Draft Results Capital Cost and Performance of New Entrant Peaking Unit

Pump selection: a real example

Southwest Clean Air Agency NE 99 th St, Suite 1294, Vancouver, WA 98682

Heat Recovery Systems and Heat Exchangers in LNG Applications. Landon Tessmer LNG Technical Workshop 2014 Vancouver

Transcription:

SCR Retrofit Improves Performance Presented by: Dale K. Purdy Sales & Marketing Manager Turner EnviroLogic 1140 SW 34 th Avenue Deerfield Beach, FL 33442 POWERGEN 2005 December 6, 2005 Las Vegas, NV

Anticipated catalyst replacement projects provide an opportune time to assess the performance of existing SCR units. A careful review of SCR system design should be made when the time comes to replace the catalyst especially if the catalyst is deactivating earlier than expected. In many cases premature catalyst failure is actually caused by poor design of the SCR system itself, which can be masked initially due to the fact that new catalysts normally outperform their guarantee for a period of time as they go through a break in stage. Effective SCR operation requires very uniform distribution of airflow and ammonia for optimal performance. Improvements can be made to both the airflow patterns and the ammonia distribution within existing SCR units that will reduce the pressure drop, improve the reduction efficiencies, reduce ammonia consumption and increase the future catalyst life. These upgrades can save money and reduce downtime. Burbank Water and Power s Lake One Power Plant Improvement Burbank Water and Powers Lake One power plant began operation on July 18, 2002. Lake One is a 47-megawatt power plant located on the grounds of Burbank Water and Power. Lake One was built to help meet the City s summer power demand. It replaces existing power plants that are as old as 25 years. The Lake One facility uses a General Electric LM-6000 PC Sprint running on natural gas. Air emissions were originally treated with a Selective Catalytic Reduction (SCR) system supplied by Hamon Research-Cottrell using CO and NOx catalysts supplied by Englehard. Operating parameters for the system are shown in the chart below. Exhaust Temperature 880 F Exhaust Flow 1,062,468 lb/hr (236,104 SFCM) CO Emissions 50 ppm NOx Emissions 35 ppm Pressure Drop Across SCR 1.8 IWC Pressure Drop Across CO catalyst 1.2 IWC Phase I CO Catalyst Replacement Very shortly after commissioning of the equipment it became apparent that Lake One was going to have difficulty meeting their permitted emissions limits, though the limits were initially achieved. The CO and NOx catalyst appeared to be degrading prematurely and was exhibiting very uneven air and ammonia distribution across the faces of the respective catalysts. This uneven flow distribution resulted in certain areas of the catalyst being over worked due to high space velocities that caused the catalyst to degrade prematurely. The uneven ammonia distribution required increasing total ammonia flow above original design in order to provide sufficient ammonia to the overloaded sections of the catalyst, which then produces excess ammonia slip rate (unreacted ammonia). As a result the facility was struggling to maintain permitted slip levels, and was using excessive quantities of ammonia, raising operating costs. 2

A review of the original design confirmed that the perforated plate sections provided for flow redistribution were inadequate. Contributing to the problems was a severe 68 degree angle in the transition from the turbine exhaust to the CO catalyst face. The photo below shows the SCR at Burbank Water and Power. SCR at Burbank Water and Power Since CO emissions seemed to be the most critical to maintaining permit compliance, Burbank Water and Power decided, after only one season in operation, to solicit bids to replace the CO catalyst as a first phase to correct their air emissions problems. The scope of the project included replacement of the CO catalyst, modifications to the existing system to improve air flow distribution and repair of the transition section from the turbine, which had become damaged due to thermal expansion. The project was to be done on a turnkey basis including fabrication of equipment, on-site modifications to the existing system, full project management responsibilities and installation. Burbank Water and Power required the following performance guarantees from the bidders of the project. CO Catalyst Replacement Project Guarantees Velocity variation of flow across the CO catalyst face and stack cannot exceed +/- 10% Back pressure at the turbine not to increase more than 1.0 IWC above current levels CO reduction of 90% must be guaranteed for 3 years at 6,000 hrs/yr Pressure drop across the catalyst must be less than 1.75 IWC Turbine must be able to operate from 5 to 50 megawatts 3

On February 18, 2004 turner EnviroLogic received a letter of intent from Burbank Water and Power to proceed with the retrofit work. The decision was based 30% on the experience and qualifications of the company and its personnel, 40% on the technical proposal offered, 20% on price and 10% on schedule. A rather tight time schedule was requested as the project was to be completed in 2-1/2 months, beginning March 1, 2004 with completion May 17, 2004. CO Catalyst Replacement Major Tasks Turner EnviroLogic s proposed solution involved several key tasks. First, the airflow distribution had to be corrected in order to achieve optimum performance, and to prevent premature failure of the replacement catalyst. Second, the catalyst blocks were to be replaced by those of a different manufacturer. Third, the transition directly after the turbine exhaust had to be redesigned to allow for thermal expansion. Airflow Distribution In order to correct the airflow problems, the existing perforated plates were removed. Perforated plates were originally employed as a means of distributing the airflow, a very common method used in many SCR designs. These plates were shown to be ineffective, especially under the wide range of air flow rates the turbine was to operate under. Perforated plates work on the principle of distribution via backpressure. When the air volume is reduced significantly under partial loading of the turbine, the backpressure is reduced to even a greater degree. Consequently, the airflow distribution capability of the perforated baffles is greatly degraded. Turner EnviroLogic decided to tear out the existing perforated baffles and replace them with distribution vanes. A system of vanes and baffles was conceived to counter the rotational motion of the turbine exhaust, slow the velocity, and provide uniform flow over the entire operating range of the turbine. The existing housing was modified to accept these components, while allowing for thermal expansion and maintenance access. Distribution vanes are much more effective at equalizing airflows over a wide range of airflow rates. Vanes are also much more effective at preventing the swirling action produced by the turbine exhaust. The plant had long experienced problems in performing compliance tests and RATA certifications, due to the location of the test ports, and flow stratification in the stack. A system of vanes and flow redistributors was designed for the entry to the exhaust stack. The vanes at the stack designed to even the airflow to improve emission testing and reduce RATA testing requirements. Catalyst Replacement The existing CO catalyst was removed and returned for recycling. The existing CO catalyst frame was disconnected and relocated further downstream, to a point immediately preceding the ammonia injection grid. This provided the extra space necessary for the flow redistribution devices. It also placed the CO catalyst in a horizontal flow section, as opposed to the previous location in a transition section. This helped provide laminar horizontal flow at the catalyst face, improving activity levels within the catalyst cells, as well as overall flow distribution. 4

The larger cross section allowed for a lower face velocity, as well as a lower space velocity, and a reduction in pressure drop. The CO catalyst was replaced by a metal monolith design with a platinum/palladium oxidation catalyst, supplied by Johnson Matthey. New Catalyst Frames After Turner EnviroLogic designed modifications to the SCR, Computational Fluid Dynamic (CFD) modeling was used to verify the effectiveness of the solutions conceived. This modeling was performed using the Fluent modeling software. A very comprehensive mathematical model was constructed, using an extremely tight matrix to achieve a fine resolution. The model was run to full convergence. Due to the size and configuration of the model, it required four processors running in parallel for twelve hours to complete each model run. The graphics presented below show the before and after conditions as determined by CFD modeling. 5

SCR Geometry & CFD Modeling Before Retrofit SCR Geometry & CFD Modeling After Retrofit 6

Transition Piece Modifications In order to maintain SCR integrity, the turbine exhaust transition piece needed to be redesigned and repaired. It had shown extensive cracking due to thermal expansion and contraction. The transition piece was originally designed as a solid housing directly contacting the hot exhaust gases. This housing was rigidly attached to the base structure and was externally insulated. As such, there was insufficient allowance for thermal expansion and the housing showed signs of cracking at the welded seams. The insulation was also being damaged as the transition piece expanded vertically. Turbine Exhaust Transition Piece Turner EnviroLogic modified the transition piece by greatly reinforcing the base and reconfiguring the lagging on the insulation so that the insulation did not get damaged when the transition piece expanded from the heat. A local contractor from Long Beach, CA was chosen by Turner EnviroLogic to do the on-site construction work. This contractor was familiar with Turner EnviroLogic having installed other SCR s for Turner on past projects. All of the components for the retrofit were manufactured at Turner EnviroLogic s facility in Deerfield Beach, FL. Equipment was completely preengineered, pre-fabricated and pre-staged to facilitate quick installation. Careful planning and experienced project management allowed the retrofit installation to be accelerated by approximately three weeks from the original schedule. The accelerated schedule was requested by Burbank Water and Power to take advantage of a time window to do other unplanned work at the power plant. Turner EnviroLogic was able to accommodate the tighter schedule. 7

Retrofit Components Staged for Quick Installation Performance Results After Retrofit The chart below summarizes the results of air flow distribution improvements. Location CFD Model before Modifications 8 CFD Model after Modifications Measurements after Modifications CO Catalyst Face 38.2 % 7.7 % 7.6 % NOx Catalyst Face 28.6 % 15.6 % 13.3 % Exhaust Stack 33.7 % 9.2 % 8.9 % As these results show, not only was the air flow distribution greatly improved but the actual tested results proved the CFD modeling to be very accurate. Removal of the original perforated baffles also reduced the system overall pressure drop significantly. Pressure drop across the CO catalyst was only 0.07 IWC and the overall system pressure drop actually decreased as a result of the modifications. Overall performance of the Lake One facility after retrofit modifications is summarized in the chart below.

Parameter Performance Guarantee Actual Tested Results CO Catalyst Velocity Distribution +/- 10 % +/- 7.6 % CO Reduction 90 % (5 ppm) 94 % (3 ppm) Pressure Drop of CO Catalyst < 1.75 IWC 0.07 IWC Turbine Backpressure Increase < 1.0 IWC Backpressure Decreased Phase II NOx Catalyst Replacement Even with the improvements in air flow distribution done in Phase I, further improvement was needed to the NOx catalyst portion of the SCR.. The newly installed CO catalyst exceeded performance requirements, allowing the plant to increase NOx water injection to the turbine to maintain compliance with permitted NOx levels. Additionally, the distribution of ammonia vapor across the NOx catalyst face was very uneven due to the ammonia header design, complicated by the complex system of valves used to balance the ammonia grid. This resulted in ammonia slip levels approaching permit maximums, and excessive ammonia usage. Once again Burbank Water and Power sought competitive bids from several qualified companies. Burbank Water and Power s proposal request only asked for NOx catalyst replacement though the responsibility for overall performance of the catalyst and responsibility for compliance with permit limits for NOx and ammonia slip was assigned to the successful bidder. Once again Turner EnviroLogic was chosen to undertake the project. NOx Catalyst Replacement Project Guarantees Guaranteed performance requirements requested by Burbank Water and Power for Phase II are shown below. NOx reduction of 90% for 5 years or 18,000 hrs of operation Pressure drop across the NOx catalyst not to exceed 3.0 IWC Ammonia slip to be less than 3.5 ppm As before, the project schedule was tight and the project was to be completed on a turnkey basis just like Phase I. There also was a lot more equipment to fabricate and install. The contract was awarded to Turner EnviroLogic on February 1, 2005 and the project work was completed on June 6, 2005. The team of Turner EnviroLogic and the local contractor, who were both now very familiar with the SCR at Burbank Water and Power, completed the project as planned. SCR Catalyst Replacement Major Tasks Field data was collected to evaluate the distribution of ammonia at the face of the catalyst, since this is critical to catalyst performance. This data, confirmed by calculations and CFD analysis, revealed that the existing ammonia distribution system was not capable of providing the distribution required for long term compliance. 9

In order to ensure equalized ammonia distribution across the NOx Catalyst face, Turner EnviroLogic recommended complete replacement of the ammonia injection grid (AIG) with a self-balancing H-header design. The effectiveness of this design had been proven by CFD analysis as well as field performance. H-Header Ammonia Injection Grid Modules The ammonia vaporization system was also inadequate for use with the replacement distribution headers. The original SCR design used 65 KW electric heaters to vaporize the ammonia. These heaters had failed several times in the past, and were not considered to be reliable. Because the heaters could not heat up quick enough to support the plant s required 10-minute start, the plant had been forced to operate them continuously. In addition to shortening heater life, this resulted in higher operating costs for electrical consumption. Recommended Changes After careful analysis, the following recommendations were made by Turner EnviroLogic. Each of these recommendations were based on the success Turner EnviroLogic has had on past SCR designs. Install new NOx Catalyst supplied by Haldor-Topsoe. Add two (2) cooling fans to lower the exhaust temperature to 800 F. Install VFD s on the fans to prevent over cooling. Install a new ammonia vaporization system that uses a slip stream of turbine exhaust to heat and vaporize the ammonia. 10

Install a new ammonia vaporization grid (AIG) designed by Turner EnviroLogic. The new AIG is self-balancing eliminating the need for balancing valves. Provide a supplemental PLC to control the system interfaced with the plant s DCS system. Ammonia Distribution Turner EnviroLogic also decided to scrap the existing ammonia vaporization system and replace it with one that uses a slipstream of hot turbine exhaust gas to vaporize the ammonia. With the new ammonia vaporization system the SCR can come online more quickly since no time is required to have electric heaters heat up. Significant electrical power savings are also realized by eliminating the electric heaters. The ammonia vaporizer was replaced with a waste heat system, designed to use turbine exhaust gas for ammonia evaporation. This system allows ammonia to be vaporized as soon as exhaust temperatures reach 300 F, which normally occurs within a minute of turbine light off. With no heaters and simplified controls, the system has proven itself to be more reliable. Performance Results After Retrofit The chart below shows the performance results after all retrofit work was completed. Load 25 % 50 % 75 % 100 % Flow Rate (dscfm) NOx (ppm @ 15% O2) Ammonia Slip (ppm) Output (MW) 150,482 171,085 174,663 184,981 Emission Limit 4.19 4.42 4.38 4.32 5.0 1.4 1.2 1.0 1.0 3.5 15 25 37 44 By all accounts both retrofit phases were deemed complete successes. Every performance requirement was exceeded and both phases were completed on or ahead of schedule. Conclusions Many SCR s that were installed in the early 2000 s may be experiencing premature catalyst deactivation. While this may appear to be a catalyst issue, it often is caused by less than optimum system design, which may be compensated for by an actual over performance of the catalyst, which occurs normally with new catalysts, before effectiveness declines to a slightly lower, long term performance level.. Careful analysis of the SCR design should be done when catalyst replacement is anticipated, to determine if system modifications should also be undertaken to maximize performance, save energy and improve system longevity, as well as extending catalyst life to meet or exceed original design parameters. 11