Radiation Control in the Core Shroud Replacement Project of Fukushima-Daiichi NPS Unit #2

Similar documents
OVER VIEW OF ACCIDENT OF FUKUSHIMA DAI-ICHI NPSs AND FUTURE PLANNING TOWARD D&D

RESEARCH REACTOR FRJ-1 (MERLIN) THE CORE STRUCTURES OF THE REACTOR BLOCK ARE DISMANTLED

Mid-and-Long-Term Roadmap towards the. Decommissioning of TEPCO s Fukushima Daiichi. Nuclear Power Station

Preliminary Lessons Learned from the Fukushima Daiichi Accident for Advanced Nuclear Power Plant Technology Development

Safety Implication for Gen-IV SFR based on the Lesson Learned from the Fukushima Dai-ichi NPPs Accident. Ryodai NAKAI Japan Atomic Energy Agency

P Boiling Water Reactor Vessel and Internals Program (BWRVIP)

Mid-and-Long-Term Roadmap towards the. Decommissioning of TEPCO s Fukushima Daiichi. Nuclear Power Station

Advanced Technologies for Fuel Debris Retrieval towards Fukushima Daiichi Decommissioning

Development of technologies for the processing and disposal of radioactive waste

Best practices for preparing vessel internals segmentation projects

Occupational Radiation Protection in Radioactive Waste Management

The 2011 Tohoku Pacific Earthquake and Current Status of Nuclear Power Stations

AREVA: Experience in Dismantling and Packing of Pressure Vessel and Core Internals

Current Status and Challenges at Fukushima Daiichi Decontamination and Decommissioning

NRA s Regulatory Perspectives on Decommissioning of TEPCO Fukushima Daiichi Nuclear Power Station

Response to Nuclear Emergency Situation - Viewpoints of Crisis Management -

Pioneer Forced Draft Cooling Tower Specifications

Atlas Chempruf TM. Coating and Lining Systems

Study on Severe Accident Progression and Source Terms in Fukushima Dai-ichi NPPs

DECOMMISSIONING PROGRAMS AND TECHNOLOGY DEVELOPMENT IN JAPAN ATOMIC ENERGY RESEARCH INSTITUTE

GENERAL CONTENTS SECTION I - NUCLEAR ISLAND COMPONENTS

WM2008 Conference, February 24-28, 2008, Phoenix, AZ Abstract #8216. Thermal Pretreatment For TRU Waste Sorting

Collection of overflowed water and soil where the overflow found has been commenced.

Inventory estimation of 137 Cs in radioactive wastes generated from contaminated water treatment system in Fukushima Daiichi Nuclear Power Station

PRESENTATION OF CONDENSATE TREATMENT

Wet FGD Materials of Construction. Gregory T. Bielawski Manager, Environmental Aftermarket Services

Nuclear Power Volume II - Nuclear Power Plants

XII. Lessons Learned From the Accident Thus Far

Nuclear Service Valves

Geothermal Power Plant

Dry storage systems and aging management

Concepts and Features of ATMEA1 TM as the latest 1100 MWe-class 3-Loop PWR Plant

AP1000 European 19. Probabilistic Risk Assessment Design Control Document

STRUCTURAL RADIATION SAFETY AT A NUCLEAR FACILITY

Read Only Copy Not For Distribution. Chapter 17. Private Potable Water Supply Systems 17.1 GENERAL REGULATIONS 17.2 QUANTITY OF WATER REQUIRED

HOW TO FACE CONCERNS OF RADIATION EFFECTS

Stainless Steel Aeration Equipment Specification

EFFICIENCY OF FORTUM'S CSTREAT AND SRTREAT IN CESIUM AND STRONTIUM REMOVAL IN FUKUSHIMA DAIICHI NPP ABSTRACT

Contents of summary. 1. Introduction

The Westinghouse Advanced Passive Pressurized Water Reactor, AP1000 TM. Roger Schène Director,Engineering Services

The Accident at Fukushima: What Happened?

Forced Draft Decarbonators. Degasification

Nuclear Power Plant Safety Basics. Construction Principles and Safety Features on the Nuclear Power Plant Level

Japan s Energy White Paper 2017

Joint ICTP-IAEA Essential Knowledge Workshop on Deterministic Safety Analysis and Engineering Aspects Important to Safety. Trieste,12-23 October 2015

Ensuring Spent Fuel Pool Safety

Nuclear Services. Put Our Expertise To Work As Your Single Source For Industrial Cleaning And System Maintenance Solutions.

The Materials Initiative NEI Overview

The principle Of Tungsten Inert Gas (TIG) Welding Process

WM2012 Conference, February 26 March 1, 2012, Phoenix, Arizona, USA

Appendix B. Aging Management Programs and Activities

HPR1000: ADVANCED PWR WITH ACTIVE AND PASSIVE SAFETY FEATURES

The Filterautomat. Our Filter Systems Protect. The New Definition of Purity for Your Medium. flow rate 5 m 3 /h to 4,000 m 3 /h. filter fineness 5 µm

Database Enhancements for Improved AREVA NP LWR Deposition Model BG Lockamon 11/17/ p.1

WM2015 Conference, March 15-19, 2015, Phoenix, Arizona, USA

The GRS Emergency Centre during the Fukushima NPS Accident: Communicating Radiological Information to the Public

SECTION COOLING TOWER

Decommissioning Group Ketut Kamajaya

Corium debris configurations in course of accident

Moisture analyzers (moisture meters) FIZEPR-SW100

IV. Occurrence and Development of the Accident at the Fukushima Nuclear Power Stations

Topics on Current Nuclear Regulation in Japan

Design of Mercury Storage Containers

Eliminating Negative Reputation Impact

Technical Strategic Plan 2016 for Decommissioning of the Fukushima Daiichi Nuclear Power Station of Tokyo Electric Power Company Holdings, Inc.

SECTION STAY-IN-PLACE INSULATED CONCRETE FORMING SYSTEM

Important. Stories on. Decommissioning. Fukushima Daiichi Nuclear Power Station, now and in the future

Status report Chinese Supercritical Water-Cooled Reactor (CSR1000)

Strategy of the decommissioning of Fukushima Daiichi Nuclear Power Station and revitalization movement of the Hamadori

DEVELOPMENT OF WET-OXIDATION TREATMENT SYSTEM FOR FILTER BACKWASH SLUDGE AND ION EXCHANGE RESINS

Steam Power Station (Thermal Station)

Nuclear Metals, Inc. (NMI) purchased undeveloped property in 1957 and the original laboratory facility was built the following year.

January 22, 2018 Tokyo Electric Power Company Holdings, Inc.

CURRENT STATUS ON THE SPENT FUEL DRY STORAGE MANAGEMENT IN TAIWAN

WM 00 conference, February 27 March 2, 2000, Tucson, AZ

Radiation Protection Challenges associated with the dismantling of Nuclear Power Plant

SUMMER 15 EXAMINATION

CHEMICAL INJECTION METHODS Pros & Cons

Fundamental Research Program for Removal of Fuel Debris

DISPOSITION OF ORNL S SPENT NUCLEAR FUEL*

Lessons Learned from Fukushima Daiichi Nuclear Power Station Accident and Consequent Safety Improvements

Innovative Process for Comprehensive Treatment of Liquid Radioactive Waste

Current Refractory Technology and Practices in the Steel Industry

Japan s Activities for Environmental Remediation after Fukushima Daiichi Nuclear Power Plant Accident

RELAP5/MOD3.2 INVESTIGATION OF A VVER-440 STEAM GENERATOR HEADER COVER LIFTING

Recovery and processing of radioactive accumulated water at Fukushima Daiichi Nuclear Power Station

Recent Technologies for Steam Turbines

Diffused Aeration Piping Equipment

Pressurized Thermal Shock Potential at Palisades

SPECIFICATION FOR SPHERICAL VESSELS (PROJECT STANDARDS AND SPECIFICATIONS)

B. System Design and Performance Requirements

(2) The work for decontamination, etc. refers to the works to remove soil, grass and trees, soil generated in association with the decontamination of

Compact, Integrated System for Coating Pipe and Tubing

Hydrosol System Furnace Cooling Water Cleaning Case Study: North American Stainless

CLEANING AND PASSIVATING OF STAINLESS STEEL EQUIPMENT

Gerhart Grinanger, NOELL GmbH, Postfach 6260, D-8700 Wizrzburg, Germany

STORAGE AND HANDLING OF NUCLEAR FUEL

Regulatory Actions and Follow up Measures against Fukushima Accident in Korea

Advanced Boiling Water Reactor

Transcription:

General Radiation Control in the Core Shroud Replacement Project of Fukushima-Daiichi NPS Unit #2 Yasunori Kokubun, Kazuyuki Haraguchi, Yuji Yoshizawa, Yasuo Yamada Tokyo Electric Power Co, 22 Kitahara Ottozawa Ohkuma-machi Futaba-gun Fukushima-pref Japan At the Fukushima-Daiichi Nuclear Power Station, Tokyo Electric Power Co., core internals have been replaced sequentially as preventive maintenance to prevent stress corrosion cracking of the shrouds. Since this work involves entry into the reactor, reduction of the collective dose equivalent and prevention of excessive exposure have been set as priority control items. Workers have to enter the reactor for installation of core internals (new shroud, etc.). In order to establish an environment appropriate for workers, various dose reduction measures (chemical internal decontamination, internal shielding, etc.) as well as development and employment of radiation protective equipment for workers have been made. These measures successfully achieved a work environment, which is observed during ordinary periodical inspection, in the reactor bottom where the great number of workers entered. From July, 1997, the world s first shroud replacement work was done at Fukushima-Daiichi Nuclear Power Station Unit #3. The collective dose equivalent was 11.5 persons.sv. For the work in Unit #2 of the same station, shroud replacement was done from August, 1998. The collective dose equivalent was 7.7 persons.sv, about 30% lower than that of Unit #3. Introduction In June 1994, a fissure caused by a stress corrosion crack was detected in the shroud main body installed in the reactor pressure vessel in Unit #2 of this station. The structure of shroud is shown in Fig. 1. Fig.1 Construction of shroud Countermeasures in this case included reinforcement of the cracked portion with brackets as well as a visual inspection every two periodical inspections on the weld line where cracks were reported frequently at all six plants. Hydrogen injection was also started sequentially in 1996. Since 1997, hydrogen injection has been done at all plants of the Fukushima-Daiichi Nuclear Power Station. In addition to these items, preventive maintenance measures to cope with stress corrosion cracking included replacement of SUS304-made shrouds in Units #1, 2, 3, and 5 sequentially with that using the material (SUS316L) that is resistant to stress corrosion cracking. Actual and scheduled replacements are shown in Fig. 2. Year 1997 1998 1999 Unit #2 Shroud Unit #5 replacement Unit #3 Fig.2 Periodical inspection process and shroud replacement plan During the 16 th periodical inspection at Unit #3 of this Station in 1997, replacement of the shroud and other core internals was achieved for the first time in the world. Though internal operations (welding, etc.) could be 1

executed automatically under remote control, workers must enter the reactor for equipment installation, checking, and inspection. Accordingly, it is necessary to improve the work environment including radiation exposure in the reactor. For this purpose, chemical decontamination in the reactor was carried out before cutting of core internals. After this decontamination, core internals were cut in water, automatically under remote control. Then, the entire reactor inside was mechanically decontaminated. Then, the radioactivated vessel near the effective core was shielded by installing a molded lead shields over the entire core area. After implementation of these measures, including chemical decontamination, the dose equivalent rate in the reactor bottom after drained decreased low enough to allow workers to work in the reactor pressure vessel. The shroud replacement project was implemented entirely within the dose equivalent limit as set forth in the applicable law (50mSv/year). The collective dose equivalent of shroud replacement work executed in the 17 th periodical inspection for Unit #2 of the Station in 1998 was about 7.7 persons.sv against the expected value of 10 persons. Sv. Since the shroud replacement project was a large-scale reconstruction over a long period of time and implemented in a high-dose-rate area, major stress was placed on assured safety of work. A radiation control plan, including mainly dose reduction, was drafted and implemented. This paper deals with the state of radiation control and painstaking efforts to reduce the dose during replacement of the shroud at Unit #2 of the Station. The state of radiation control Before starting shroud replacement, an overall plan concerning radiation control was drafted for positive checks of individual items before proceeding to the next step. (1). Collective dose equivalent The collective dose equivalent for shroud replacement was added to the total dose of 10 persons.sv by considering the work environment for individual activities and by estimating the dose for each job title from the work period and man-hour. Concerning the collective dose equivalent of shroud replacement, the actual value of core shroud replacement, feedwater sparger and core spray line replacement, nozzle safe end replacement, and auxiliary works (cutting core internals into pieces) was below the expected level. The collective dose equivalent was 7.7 persons.sv as compared to the expected value of 10 persons.sv. We believe that chemical decontamination and internal shield were combined effectively with the painstaking efforts for reduced dose in each activity and contributed to reduction of the dose by about 20%. (2). Individual workers dose control As workers have to enter the reactor for equipment installation, checking, and inspection, thorough dose equivalent control was done for individual workers. Through painstaking dose control of individual workers, the individual dose equivalent of about 2300 workers engaged in shroud replacement was less than one half of the legal limit of annual 50 msv. We planned the individual dose per day to be maximum of 5 msv, but the actual dose was less than the planned level. Implementation of Dose Reduction Measures Fig.3 shows the status of implementation of major dose reduction measures. The fuel assembly, control rod drive mechanism, dryer, and separator were taken out of the reactor according to the ordinary procedure. Fig.3 Implementation of principal dose reduction measures First, chemical decontamination was done to remove radioactive materials accumulated in the reactor, followed by submerged cutting and removal of core internals for disposal. Chips and residual crud left after cutting were removed by mechanical decontamination using brush and water jet in water under remote control. The highly-radioactivated reactor internal wall surface, etc. was shielded in the water. Subsequently, water was drained to establish the atmospheric environment where the workers could be engage in activities. Then, the work with automatic remote devices, flushing, and additional shielding (if necessary) was made. Mock-up training, reduction of work man-hours, and further careful dose reduction measures were implemented. 2

(1) Chemical decontamination The CORD/UV method was employed for chemical decontamination, in which oxidization and reduction are repeated with oxalic acid and permanganic acid (decontamination reagents) to dissolve and remove crud produced and adhering to the equipment and piping inside. The CORD/UV method is outlined in Fig.4. Fig.4 Chemical decontamination system The water was circulated by temporary equipment and piping and radioactive materials were removed with ion exchange resin. Decontamination steps were taken for three cycles. Before implementation, the cycle progress logic was prepared, with the judgment criteria established to determine if the work could proceed to the next step. In each cycle, various monitoring was conducted to see if the target DF(Decontamination Factor) had been achieved. A high-temperature radiation monitor (NaI(Tl)) was inserted in three locations, periphery, middle point, and center of a housing of the control rod drive mechanism, monitoring continuously the transition of dose equivalent rate below the water line in the reactor bottom. The dose rate on the piping surface of the reactor recirculation system was measured with an ICW survey meter before and after decontamination. Finally, the system water was sampled at the outlet of the resin tower to monitor the radioactivity, metallic oxides, and concentration of decontamination reagents. The monitoring method and results of chemical decontamination is shown in Fig.5. Fig.5 The monitoring method and results of chemical decontamination Decontamination proved effective, exceeding the target DF20. Namely, the removed radioactivity was about 10 TBq. The average dose rate in the water on the reactor bottom was at a ratio of 108 before and after decontamination, and the average dose rate on the piping surface of the reactor recirculation system was at a ratio of 68 before and after decontamination. (2) Mechanical decontamination After the cutting and removal of core internals, mechanical decontamination was conducted through repeated brushing, suction, and water spray in the reactor. The target was set for each step and decontamination method, and the effectiveness was confirmed. (3) Shielding of the reactor inside the wall 3

Shielding was provided for the highly-radioactivated reactor wall and for the reactor bottom where radioactive materials tend to accumulate. For the reactor wall, 36 pieces of 7 m high and 3 ton weight shields were provided. Each shield consists of the 80 mm thick lead covered by 5 mm thick stainless steel. The reactor wall shield is shown in Fig. 6. Fig. 6 The reactor wall shield The reactor bottom was provided with a 25 mm thick stainless steel shield. With these measures, the dose rate in the air was reduced ensuring the environment where the workers can be engaged in activities. (4) Flushing To remove crud accumulated in the piping nozzle thermal sleeve at the recirculation inlet (N2), feedwater (N4) and core spray (N5), water jet cleaning was used, achieving reduction effectively by about 31 88%. These measures were to reduce the dose during replacement of the nozzle safe end in the Primary Containment Vessel(PCV). Fig.7 Effects of thermal sleeve jet flushing (5) Painstaking dose reduction The radiation control group took a leadership to reduce the dose during shroud replacement. Examples of dose reduction measures and developments appropriate for the site are introduced below. a. Dryer cleaning and shielding around the dryer The dryer and separator are stored in water at the D/S storage pool during ordinary periodical inspections. To secure the area for cutting core internals at the D/S storage pool, the dryer and separator are stacked in two stages, allowing a 2.0 m portion of the dryer to be exposed to the air. Though a 50 mm steel plate is provided for entire coverage, it was confirmed that the environmental dose rate of the operation floor(working area) as a whole, including the area for cutting of core internals, increased. Accordingly, mechanical cleaning was done on the dryer which is partially exposed to the air, reducing successfully the dose rate by about 30%. Moreover, as far as the floor load capacity of steel plate shield allows, lead mats were temporarily installed on the top and on the sides. Dose reduction by about 65% was achieved. b. Development of nozzle shape shield and lead-clay shield For replacement of the nozzle (N2) safe end at the recirculation piping inlet, a shield appropriate to 4

the nozzle shape was developed by taking into account flexible shielding, reduction of the installation time, and prevention of displacement after installation. As a result, the installation time was reduced to one-fourth of the conventional time. In addition, the lead-clay shield in which the lead is sandwiched by clays was developed, which was packed into the cut end of N2 piping inside from the PCV side to reduce the effect from the reactor inside. Implementation of work safety measures In order to ensure work safety and to suppress the release of radioactivity to the surrounding area, several measures were implemented. (1) New equipment for workers Concerning the equipment used by workers, a welding hood mask was developed for activities using fire in the reactor (welding, etc.). In addition, a water-covered hood mask was developed and used for removal of thermal sleeves in the pedestal. And a water-proof permeable protector was developed. These equipment reduce greatly the physical load on workers. (2) Implementation of work without a mask in the reactor After installation of the new jet pump, the surface contamination density of the work area was controlled to a level less than that at which the mask must be worn through decontamination and protection of the reactor inside. In consequence, the welding operation, etc. of the sensing line could be done without wearing a mask. Even after installation of the new shroud in the reactor, the workers could operate without wearing the mask. In this way, improved efficiency could be achieved with reduced work time, and we successfully achieved the reactor environment which is observed outside the reactor. The reduction achieved through these painstaking control measures is estimated to be about 2.3 persons.sv. As compared to the expected collective dose of 10 persons.sv, the actual dose equivalent during shroud replacement was 7.7 persons.sv. Conclusions On the basis of knowledge obtained during shroud replacement in Unit #2 of Fukushima-Daiichi Nuclear Power Station, we would like to continue positive implementation and evaluation of chemical decontamination while continuing painstaking radiation control for Unit #5 in progress. Stress continues to be placed on safety against radiation. 5