My Home Industries Pvt Ltd., (An ISO 9001:2008, ISO 14001:2004 and OHSAS Certified Company) Mellacheruvu Nalgonda District (Telangana)

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My Home Industries Pvt Ltd., (An ISO 9001:2008, ISO 14001:2004 and OHSAS -18001 Certified Company) Mellacheruvu 508 246 Nalgonda District (Telangana)

Company Profile My Home Industries Pvt Ltd (MHIPL) is established in the year 1998 with an installed capacity 0.2 mtpa and rose to 8.5 mtpa in Andhra Pradesh and Telangana states. MHIPL entered into a JV with CRH Plc, Ireland in 2008,an internationally reputed group having the business in cement and building materials in 35 countries. Other core businesses of the group are Construction & Real Estate, Power, Transport, Power Consultancy,Medical and Education. MHIPL is an ISO 9001:2008, ISO 14001:2004, OHSAS 18001 certified company.

Present Production Capacities Details Particulars Unit-I Unit-II Unit III Total (MT) Present capacity Clinker 0.660 1.183 1.20 3.043 Cement 0.792 1.108 1.40 3.30 Capacities in million tonnes per annum Unit-II Unit-III Unit-I

Production Technology applied Dry Process of Cement Manufacturing Technology Three units are set-up with state-of the-art technology from Walchand Industries, KHD Germany and FLSmidth, Denmark. Online x-ray analyzers ensure quality at every stage of manufacture. Fuzzy logic system operates all the equipment with total automation to ensure consistent quality.

Best practices adopted for utilization of AFR Usage of alternative fuels (pharmaceutical waste) in kiln Usage of petro polymer fuel(ppf) for kiln light ups in place of Diesel.

Co-processing at MHIPL System installed and commissioned in March 12 Facility designed by FL Smith, Denmark, considering safety & environmental aspects as per CPCB guidelines ( HAZOP study was conducted by M/s Chola, Chennai) System is designed to handle and fire spent organic solvents along with coal in Kiln and Pre calciner burners. Total project cost about 12 crores.

Salient Features of Co-Processing System Liquid HW Storage tank Storage tanks - 2 Nos. double walled made of SS 304, each of 100 KL capacity. Continuous online level sensors provided for monitoring the quantity of solvents stored.

Liquid HW Pumping System Unloading pumps - (1+1) 25 m 3 /hr capacity with flame proof motors. Feed pumps - (2+1) 5 m 3 /hr capacity with flame proof motors. Unloading pumps Solvent feed pumps

HW firing system in Kiln MF( Multi Fuel) station for regulating & monitoring solvent flow with atomizing air Burner stations of capacity 3000 kg/hr with pipe & fittings in SS 317 Multi Fuel System

Fire Hydrant Systems at AFL Storage Fire Hydrant system Foam type - 273 cum/hr @ 7.0 Kg pressure. Temperature sensors provided around the tank to monitor surface temperature. With increase of surface temperature the Fire hydrant system automatically starts.

Nitrogen System Nitrogen Blanketing (Safety systems) Nitrogen Generator system of 30 Ncum/hr capacity for blanketing while unloading and pumping of liquid waste. Uses: This will eliminate the fire hazard even at elevated temperatures. This also does not allow solvent vapors to vent out because of positive nitrogen pressure(150-200. mmwg).

Problems Faced after commissioning Receiving quality of AFL is main concern, while pumping the liquid from storage tank to user end. Viscosity and Net calorific values are main quality concerns and affect the Feeding rate and system efficiency. Due to the variable viscosity and calorific value in AFR, effects the clinker burning process. Odour at some times emits from storage Tank vent.

Actions Initiated AFL Laboratory Modified Filters are provided in transport pipe lines. Spray system improved by changing the burner gun from OBA40 0 to OBA60 0 nozzle. AFR firing shifted from Kiln PC to setup alternative fuel Laboratory for analysis of flash point, Viscosity,CV and other & Minor constituents, etc.

Scrubber system for odour control Installed Dry & Wet Scrubber to avoid odour emissions from the storage tanks to atmosphere. Invested 50 Lakhs.

Typical analysis of (Spent Organic Solvents) utilized for Co-Processing. Sr. No. Parameters UOM Liquid Waste Proximate Analysis 1 Moisture Content % 0.81 2 Ash Content % 1.43 3 Volatile Matter % 95.68 4 Fixed Carbon % 2.08 Ultimate Analysis 1 Carbon % 43.94 2 Hydrogen % 7.31 3 Nitrogen % 5.59 4 Sulphur % <0.1 5 Mineral matter % 1.44 6 Oxygen % 41.62 7 GCV Kcal/mol 3500-5855 8 Chloride as Cl % 0.02

Efforts made for increase AFR TSR% 2016-17 Environment Lab installed to monitor quality 2.75 2015-16 2014-15 Firing shifted from Kiln to PC in Kiln-3 Firing shifted from Kiln to PC in Kiln-2 1.60 2.48 2013-14 2012-13 AFL Burner Gun modified 0.93 AFL Commissioned March 12 1.49

REDUCTION IN CO2 EMISSIONS DUE TO AFR USAGE

WAY FORWARD To achieve the AFR utilization 5% with in 3years and 10 % with in 5 years on TSR basis. Planning to install AFL system for Line-1 also. By feeding 1000 kg/hr in unit-1,we can achieve Solid AFR feeding 5% AFL utilization on TSR basis Developing the in-house solid waste feeding system, which is already in Progress. Maximum utilization of waste generation with in the plant and surrounding areas Proposed AFL in Line-1

UTILIZATION OF PETRO POLYMER FUEL Substitute of Diesel firing Used for Kiln Heat up Petro polymer fuel generated from plastic waste 1MT fossil Fuel produces 3 MT of Carbon Dioxide (CO 2 emission). By using this PPF we are reducing CARBON FOOT PRINT. DIESEL Calorific Value 10000 Kcal/Kg High NOx and CO emissions Does not meet green environment norms Net CO2 emissions = 3 tons per ton of Diesel fired PPF Calorific Value 10250 Kcal/Kg Low NOx and CO emissions Meets green environment norms Net CO 2 emissions = zero Made from CRUDE OIL Recycled Fuel from Waste Plastics

REDUCTION IN CO2 EMISSIONS DUE TO PPF USAGE Co2 Reduction in MT/YR 98 42 2015-16 2016-17 GHG emissions reduced by 98 MT CO2 during the year 2016-17.

Conducted KEP 2 nd WORK SHOP ON BEST PRACTICES in ENERGY EFFICIENCY under Cement Sector on 07&08 th June 16

AWARDS GREENTECH SAFETY AWARD 2013 GREENTECH ENVIRONMENT AWARD 2013 EHS AWARD 2013 MOST PROMISING BRAND 2014-15 BEST MANAGEMENT AWARD 2015

17 th CII National Energy Efficiency Award-2016

Organization Recognition Award in 30 th Chapter Convention in Quality Circle(CCQC)-2016

The India s greatest brands & leaders Award 2015-16 *Pride Of The Nation* instituted by United Research Services(URS).

..aiming to conserve natural resources