COPYRIGHT. Development of a Gas Condensate Reservoir. The Anschutz Ranch East Field: Case Study

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Development of a Gas Condensate Reservoir The Anschutz Ranch East Field: Case Study SPE 10992, 11968, 12042, 12257, 13108, 14412, 14414, 14456, 22824 The Anschutz Ranch East Field Located in the Western US Overthrust Belt Wyoming Utah border Structurally Complex Area More than 350 dry holes drilled before Pineview Field discovered in 1975 Fields are Anticlinal Structures Along the Hanging Wall of Thrust Faults 1

Overthrust Belt Field Map Original Field Prospect Map 1979 2

Field Discovery Bountiful Livestock No. 1 spud March, 1979 Authorized total depth 11,500 feet Encountered Nugget reservoir target 3,000 feet deeper than forecast Penetrated over 940 feet of gross thickness Completed December, 1979 128 ft of perforations below 13,000 ft IP 3.9 MMcfd, 1,054 BCPD CGR 270 bbl/mmscf Post Discovery Interpretation 1500 Acres 3

Additional Drilling Reveals a Bigger Prize Offset drilling indicated original structure was larger Anschutz 12-26 Spud January, 1980 encountered separate Nugget structure 2,000 feet deeper Well completed December, 1980 Perforations below 14,750 feet IP 0.88 MMcfd, 96 BCPD CGR: 109 bbl/mmscf January, 1981 Interpretation 14,600 Acres 4

Additional Development Results One Reservoir or Two? Observations: Delineation drilling on the east lobe proved smaller areal extent Revised interpretation in 1982 decreased total area to 3,900 acres West lobe has over 2,100 feet of hydrocarbon column Estimated 2 Tscf gas-in-place Different Gas-Water Contacts Different Reservoir Fluid Properties Implications: One Reservoir or Two? Geological data suggests that the two reservoirs are connected by the overturned Nugget Section as shown in the X-Section. 5

Cross Section Showing Overturned Nugget 1982 Interpretation 3,900 Acres 6

Anschutz Ranch East Rock Properties Nugget Sandstone Triassic Jurassic age Desert sand dune environment 1,050 feet average gross stratigraphic thickness 70 90 percent net-to-gross ratio Porosity: 2 to 22 % Avg. Near 10% Permeability: 0.1 to 1000 md Avg. 3 md Reservoir grossly correlates into 3 major zones Data Bank Well logs Resistivity, porosity, dip meter Cores Several thousand feet Fluid samples More than 20 recombination tests Multiple depths in multiple wells Pressure Buildup Tests Repeated with time in several wells 7

Anschutz Ranch East Nugget Type Log Nugget Porosity by Zone 8

Nugget Permeability by Zone Reservoir Fluid Properties Rich gas condensate Substantial compositional variation with depth Slightly undersaturated Dew point pressure 150 350 psi below initial reservoir pressure Pressure depletion data (PVT) shows significant liquid drop out below dew point 20 40% percent of hydrocarbon PV 9

West Lobe Condensate Samples Deep Compositional Gradient Fluid Properties Vary With Depth Shallow Elevation, ft subsea -4,400-5,324-6,400 Reservoir Pressure, psi 5,150 5,310 5,490 Dew Point Pressure, psi 4,920 5,080 5,165 Gas-Oil Ratio (scf/stb) 5,639 4,561 3,523 Maximum Liquid Dropout, % 20.5 26 37.5 10

Field Development Issues What are the technical options for developing and producing this reservoir? Arrange options in descending order of recovery for the condensate gas. How would you develop this reservoir under each option? What tools would you employ to investigate risks and rewards? Field Development Plan (FDP) Issues Production mechanisms Depletion Full pressure maintenance (FPM) Partial pressure maintenance (cycling) Injection fluid Lean gas, rich gas, nitrogen, CO 2, flue gas Injection/production well pattern Well spacing Completion philosophy 11

Initial FDP Reservoir Models (1981 1983) 2-D Compositional Cross-Section 17 Components, 6 Layers (Various Descriptions) Evaluate Depletion Strategies 3-D Black Oil Field wide HC Gas and N 2 Fluid Properties, 4 Layers (A really Homogeneous) Evaluate Injection Pattern and Well Spacing 3-D Compositional Pattern 11 Components, 6 Layers (Various Descriptions) Evaluate Injection Fluid Composition, Buffer Size, Pattern Sweep and Spacing 3-D Compositional Field wide 9 Components, 4 Layers Both Homogeneous and Heterogeneous Cases Validate Forecasts Using Superposition of Pattern Model Initial Development Plan for West Lobe (Based on Simulation Studies) Produce under full pressure maintenance Drill on 80-acre well spacing Use inverted 9-spot well pattern Complete wells selectively Producers: Lower 2/3 of formation Injectors: Upper 2/3 of formation Inject 10% HCPV buffer of 35% N 2-65% HC gas followed by pure N 2 50 MMCFD of N 2 provided by air separation plant 12

Initial Development Plan for East Lobe Produced Under Pressure Depletion The liquid yield is too low to economically justify developing this part of the reservoir under a Full Pressure Maintenance Scheme It may have offered an economic incentive under a gas cycling scheme, however Why an Inverted 9-Spot Pattern? Depositional environment resulted in NW-SE permeability trend Structural deformation and fracturing had caused anisotropy in a different direction Inverted 9-spot pattern allows subsequent conversion to suitable line drives of different orientations 13

One Possible Conversion: 9-Spot to Line Drive Development Timeline 12/82 6/83 12/84 1985-1986 1985-1986 Begin full field production upon unitization N 2 breakthrough in four wells Second 50 MMCFD N 2 plant operational Convert to line-drive pattern Depositional permeability trend was dominant Workovers to open Zone 1 in producers Try to improve reservoir sweep 1/86 12/87 8/88 Maximum condensate production 45,968 BPD NGL/NRU operational (increase NGL sales) HC gas sales limited by market conditions Development drilling complete West Lobe 29 Prod, 18 Inj East Lobe 7 Prod 14

Final Structure Map Showing Line Drive Pattern West Lobe Production History 1000000 100000 10000 1000 100 10 1 Inj. (MCFD) Prod. (MCFD) Gas Sale (MCFD) NGL (BPD) Cond. (BPD) GOR (MSCF/Bbl) Prod. N2 (%) Inj. N2 (%) Jan-81 Jan-82 Jan-83 Jan-84 Jan-85 Jan-86 Jan-87 Jan-88 Jan-89 Jan-90 Jan-91 Jan-92 Jan-93 Jan-94 15

Reservoir Performance Falls Below Expectation Recovery forecast is substantially lower than forecasted by the 1983 simulation studies Possible cause is poor sweep efficiency High permeability streaks/fractures in zones 1 and 2 resulted in pre-mature breakthrough Low permeability in zone 3 resulted in minimal production contribution What Next? What are your options for the continuation of this project? How would you investigate these options? 16

Technical Options Wellhead Compression Well Stimulation Program Solvent injection for removal of condensate banks Selective hydraulic fracturing in Zone 3 Horizontal well drilling in Zone 3 Reservoir Simulation Studies New 1990 1994 simulation studies, incorporating improved reservoir description, fluid characterization, and better computing hardware/software Conclusions of 1990 94 Simulation Studies Continued FPM is not economically attractive Produced N 2 cut will increase rapidly Decline in condensate production will continue Sweep improvement options are costly Field wide partial pressure maintenance is inefficient and economically unattractive Blowdown is economically attractive with risk Water influx is not known 17

West Lobe Blowdown 10/92 Initiate blowdown pilot in North End of field and increase gas sales 6/83 12/84 Increase additional gas sales using makeup nitrogen Decrease injection and initiate field blowdown Maintain 100 MMCFD of N 2 injection in 4 down-dip wells to retard aquifer influx 4Q/98 Stop Injection and Begin Full Blowdown West Lobe Blowdown Performance Rates, bbl/day or Mscfd 1000000 100000 10000 1000 Anschutz Ranch East West Lobe Blowdown Performance 100000.0 10000.0 1000.0 100.0 Well Count or Ratios, bbl/mmscf Cond Gas Water CGR WGR Prod Wells 100 10.0 10 1.0 Jan-94 Jan-99 Jan-04 Dec-08 Jan-14 Date 18

Cumulative Production and Recovery Factors Jan 1997 West Lobe Cumulative Production 112.2 MMbbl cond (121.6 MM Nov 2011) 91 MMbbl NGL 289 Bcf HC gas Expected Ultimate Recovery Factors Summary Cond 38% (would have been <20% under pressure depletion) NGL 65% HC Gas 60% The FPM plan was both technically and economically successful Reservoir heterogeneity had a large impact on rate/recovery performance Poor sweep resulted in earlier-than-expected nitrogen breakthrough and lower-than-predicted condensate recovery The flexibility to modify development plans based on field performance was critical to maximizing profitability of the project. 19

Question What would you do differently today? 20