SHOULD WE KEEP DO FOR NITRIFICATION CONTROL?

Size: px
Start display at page:

Download "SHOULD WE KEEP DO FOR NITRIFICATION CONTROL?"

Transcription

1 SHOULD WE KEEP DO FOR NITRIFICATION CONTROL? THE PROOF IS IN THE AMMONIUM ELECTRODES Robert Lagrange 1 *, Sue Baert 2, Amanda Poole 3, Dave Green 3 and Nick Camin 4 1 Lagrange Consulting, 4310 Royal Mustang Way, Snellville, Georgia, USA, (*correspondence: rplagrange@gmail.com) 2 Wheaton Sanitary District, 1S640 Shaffner Road, Wheaton, Illinois, USA, Baxter & Woodman Inc., 39 South LaSalle Street, Suite 816, Chicago, Illinois, USA, Endress+Hauser Inc., 2350 Endress Place, Greenwood, Indiana, USA, KEYWORDS Process Control, Optimization, Nitrification, Ammonium, Dissolved Oxygen, Energy Consumption, Compliance, Instrumentation ABSTRACT Aeration often is the process that consumes the most energy in a wastewater plant. At the same time it is an essential process to maintain compliance for BOD and Ammonia limits. It thus deserves a lot of attention. The use of dissolved oxygen measurement to control aeration is widely accepted. The literature has many examples of excellent return on investment in wastewater plants that have implemented this control. There are even theories that a concentration of 2 mg/l is the perfect value. But a DO sensor only tells how much oxygen has not been used in the process and at times this measurement may not bring the expected results. The effluent may end up out of compliance or too much energy can be spent. Examples are available. As one of the main objectives of the aeration tank is nitrification the measurement of the concentration of ammonium or ammonia provides much better information than dissolved oxygen. Ion Selective Electrodes (ISE) installed directly in the tank eliminate the need for sampling line and ensure an easier integration. Their selectivity, accuracy and lower maintenance make them an attractive solution. As demonstrated at Wheaton and Colorado Springs, additional energy savings and compliance are possible when using either ammonia in a cascade loop with DO control or in direct control of the air flow. Direct control either in feed-forward or feed-back provide faster and better response when spikes are present. The return on investment is very good even on smaller plants and compliance is achieved. Dissolved oxygen concentration remains an important factor as it affects the quality of the sludge. The control strategy has to maintain it within limits.

2 Lagrange, Baert, Poole, Green & Camin 2 INTRODUCTION Many wastewater plants around the world are working hard to reduce their energy consumption and the amount of nutrients discharged in their effluents. As both carbon removal and nitrification consume oxygen it is important to insure that oxygen is present in the right amount in the aeration tank. Dissolved Oxygen Instruments (DO) are typically used for this application. But they are only an indication of the amount of free oxygen available at the measuring point. The measurement of the amount of air sent to the tank provides the additional data to determine the oxygen uptake rate. In this paper the data from Wheaton Sanitary District (Illinois) provides the base for the discussion and data from other sources will be added to confirm the findings: the installation of instruments for automatic control is justified for small to large plants. THE GOOD AND THE BAD OF DISSOLVED OXYGEN MEASUREMENT The good The literature abounds in examples of plants using DO to control the airflow to the aeration tank. The return on investment is good even for small plants. Eagle Lake Sewer Utility District in Wisconsin treats only 0.26 MGD and was able to justify the installation of an optical DO instrument with the additional benefit of reduced maintenance cost (Kohlmann, 2010). As water and wastewater consume about 4% of the energy produced in the USA, power companies have shown a big interest in promoting DO control associated with blowers with Variable Frequency Drive (VFD). The Tennessee Valley Authority (TVA) sponsored demonstrations in real life at existing wastewater plants. A result is shown in Figure 1.

3 Lagrange, Baert, Poole, Green & Camin 3 Figure 1 TVA demonstration The Installation of DO sensors and VFD s provided a 13% reduction in consumption and most importantly a 39% reduction in peaks with the corresponding rate change.. More recent data shows that reduction in consumption of up to 50 to 60 % can be achieved and 80% when new diffusers are used (Poole, 2011) The bad As we said earlier DO only shows the residual amount of oxygen available in the tank. It certainly does not define the elimination of carbon nor does it tell precisely what is happening with nitrification or denitrification. The Hanover Area Regional WWTP (Pennsylvania) installed Ion Selective Electrodes instruments in their oxidation ditch. For the initial period the data, Ammonium and Nitrate concentrations, were recorded but not available to the operators. They had the information from a flowmeter, a DO and a NADH (Fluorescence of nicotinamide adenine dinucleotide) to operate the plant. The surface aerators had only 2 speeds. (Lagrange, 2009) Figure 2 shows the location of those instruments at about 1/3 rd of the tank.

4 Lagrange, Baert, Poole, Green & Camin 4 Figure 2: Location of the instruments at Hanover Figure 3 Hanover Data Figure 3 shows the data for almost a week of operation. In the initial part the DO value does not change while both the flow and the ammonium concentration (scaled 0 to 15 mg/l) change. As a result the effluent was out of compliance. Then the aerator speed is finally adjusted between high and low to follow the diurnal flow variations. The ammonium concentration is drastically reduced. Too much in fact as at 1/3 rd of the ditch it is already below 2 mg/l. The plant was expecting to see some denitrification taking place at low aerator speed (nitrate concentration scaled 5 to 25 mg/l). Again it is not happening. The plant was using far too much energy.

5 Lagrange, Baert, Poole, Green & Camin 5 EXPERIENCE AT WHEATON SANITARY DISTRICT The Wheaton Sanitary District is also looking at ways to maintain or improve the quality of its effluent while reducing the consumption of energy. A new turbo blower was installed in 2011 to replace an existing multistage centrifugal blower. Then a joint project was started with Baxter & Woodman to find the best control strategy for that specific plant. Endress+Hauser Inc and WTW (now Xylem) provided instrumentation assistance for the project. The plant is designed to treat a dry weather flow of 8.9 million gallons per day (MGD), a design maximum flow of 19.1 MGD and a peak wet weather flow of 45 MGD. The effluent is discharged in Spring Brook with very low flow that dictates the willingness of the District to discharge effluents with a quality well above their discharge permit. The treatment consists of screens, sand, grease and fat removal, primary clarification, trickling filter, aeration, secondary clarification, filtration and disinfection. The District has 5 aeration tanks in parallel. Each equipped with one Air Flow measurement and one DO measurement. For the test one Ion Selective Electrode (ISE) based measurement for ammonium was installed toward the start of tank 2 and another at the end of tank 3 Figure 4: Wheaton aeration showing the location of the instruments

6 Lagrange, Baert, Poole, Green & Camin 6 Step 1 Air Flow Control After the installation of the new blower the first step was to maintain a constant air flow to each tank. With this in place the DO concentration keeps changing reverse tracking the ammonium concentration measured close to the inlet in tank 2 as expected. During that time the ammonium concentration in tank 3, measured close to the end of the tank, remains constant around 0.4 mg/l very close to the limit of detection of the instrument. This confirms that nitrification is complete. In the final effluent, after some post aeration, the ammonia concentration is at a non detectable level in laboratory samples (<0.05 mg/l) Figure 5: Tank2 in airflow control mode A 28% energy consumption saving was achieved, 10% of which can be attributed to the control itself Step 2 DO Control In that phase the control objective is to maintain a constant DO. With the correct DO set point there should be enough air to keep the solids in suspension and prevent settling in the aeration tank.

7 Lagrange, Baert, Poole, Green & Camin 7 In that period, as can be seen in figure 6 there were some ammonium spikes the largest and with highest rate of increase was on January 14. The control reacts well with that spike. As the DO measurement is located toward the end of the tank, some 20 feet, the control had difficulty to keep up with the fast change resulting in a very small blip on the effluent ammonium measurement. The change is less than 0.2 mg/l increase. There was a 9% increase in energy consumption compared with the period with airflow control. Figure 6 DO Control Step 3 Ammonium Control Figure 7 compares tank 2 in ammonium control with tank 3 in airflow control. The variations in DO concentration are drastically reduced and in tank 3 the process remains under control with the big spike

8 Lagrange, Baert, Poole, Green & Camin 8 of ammonium on January 28/29. At the same time with the same wastewater in tank 3 the oxygen is completely depleted and the nitrification is not complete. The use of ammonium in feed-forward provides a better control, more stable process and insures that the concentration of ammonia in the effluent remains at the low level desired by Wheaton. Figure 7 Feed forward NH4 control ISE A BETTER TOOL When normalizing for changes in flow and BOD load the results favor ammonium control Step 2 consumes 5% more energy Step 3 consumes 6% less energy. From Wheaton s point of view achieving a stable process while maintaining their very low ammonia discharge justified the investment to install one ISE instrument in the splitter box ahead of the 5 aerations tanks and modify the control strategy to feed-forward control. The decommissioning of the

9 Lagrange, Baert, Poole, Green & Camin 9 trickling filters will bring a higher nutrient load to the aeration tank allowing for a more efficient control as the low limit on air flow from the blower will be prevented. As we can see in figure 7 there is margin to reduce the energy consumption. Colorado Springs Utilities Colorado Springs Utilities (Lagrange, 2011; Camin, 2011) with a different set of problems took a different approach. That plant faces very high daily ammonia peak while trying to run only their small compressor. Designed for 20 MGD the actual flow was only 8 MGD at the time of the study, While on DO control (those DO units were installed at construction time) the plant faced some high ammonia concentration in the effluent or at other times low ph as nitrification consume alkalinity. The decision was then made to install ISE measurement for both ammonium and nitrate as some denitrification was implemented to increase alkalinity. The locations are described in figure 9. Figure 8 Concentration of influent ammonia in green and power consumption at CSU

10 Lagrange, Baert, Poole, Green & Camin 10 Figure 9 Installation point for the instruments at CSU To increase the speed of response of the control loop the air flow is directly controlled based on the ammonium concentration. The control takes into account the DO concentration to maintain it within high and low limits. With that control strategy CSU was able to reduce the cost of energy while the flow increased as shown in figure 10 for the months of November 2009 and November 2010.

11 Lagrange, Baert, Poole, Green & Camin 11 Figure 10 CSU flow and cost The consumption of energy per MGD per pound of ammonia nitrified was reduced by 12% compared with standard DO control. In the future the Ammonium sensor after the primary will be relocated to the swing zone to combine feed-forward and feedback. Others The city of Peoria, Arizona, operated their Beardsley Road Water Reclamation Facility, a 4 MGD plant, with a cascade control where the output of the Ammonium controller adjusts the set point of the DO control loop. They were able to achieve a 3 months return on investment and improve the sludge quality. (Dabkowski, 2011) Rieger (2012) also demonstrated in three wastewater plants with average flows of 3.5, 10.5 and 54 MGD in Switzerland that the use of ammonium control provides benefits on other processes such as a reduction in the consumption of chemicals for phosphorus removal as more volume can be used in anaerobic phase.

12 Lagrange, Baert, Poole, Green & Camin 12 SUMMARY Wheaton Utilities District decided to use a control strategy based on feed-forward based on ammonium concentration as it provides them with the best results for their objectives. Colorado Springs used a partial feedback and achieved excellent results. Peoria included the ISE in a cascade control for a high return on investment. Further reading is available. (Grievson, 2012) We would like to leave the final comments to Leiv Rieger Ammonia controlled aeration in an activated sludge system leads to a significant reduction of the total energy consumption in conjunction with decreased effluent concentrations of total nitrogen..the best solution will be the simplest concept that still yields a significant benefit in comparison with the annual costs. LIST OF ACRONYMS: ISE... Ion Selective Electrode DO... Dissolved Oxygen NADH... nicotinamide adenine dinucleotide (fluorescence of) CSU... Colorado Springs Utilities MGD... Million Gallons per Day

13 Lagrange, Baert, Poole, Green & Camin 13 REFERENCES Camin & al. Ammonia Based Aeration Control Workshop 105 WEFTEC 2011 Dabkowski & al. Ammonia Based Aeration Control Workshop 105 WEFTEC 2011 Kohlmann. Saving costs by continuous monitoring of D.O. in plant Application Note Endress+Hauser Inc Grievson Aeration Control in wastewater activated sludge plants using mixed liquor, organic loading and ammonia analysis Water Industry Process Automation & Control Group, March Lagrange & al. The revival of the Ion Selective Electrode Applications in Wastewater Plants ISA Expo 2009 Lagrange & al. A change in control strategy reduces power consumption at Colorado Springs Utilities Energy & Water 2011 Poole & al. Aeration System Automation: Control Strategies to Maximize Energy Savings at Low Capital Cost WaterCon 2012 Rieger & al. Improving Nutrient Removal While Reducing Energy Use at Three Swiss WWTPs Using Advanced Control Water Environment Research, Volume 84, 2012

14 Lagrange, Baert, Poole, Green & Camin 14 About the Authors: Robert Lagrange, PhD is a Doctor in Physics from the University of Grenoble, France. After 11 years with Endress+Hauser as Business Manager Water and Wastewater Robert is now working part time as a consultant. Robert presented multiple times at the ISA WWACS and is a member of WEF and AWWA instrumentation and control committees Sue Baert, B.Sc. is the Plant Superintendent at the Wheaton Sanitary District where she started as a chemist became the Lab Manager and wrote the Quality Assurance Project Plan for the stream water quality project, collected, analyzed and submitted the data. She has a degree in Biology/Chemistry from the UW-Lacrosse. Sue is involved with the DuPage Salt Creek watershed group as Vice- President. She is an active member of WEF through the local MA Central States Water Environment Association (CSWEA). She was President of the Illinois section of Central States for a one year term, and then Illinois Trustee to the Executive staff for two years. In all, her career in the water/wastewater section has spanned over 22 years. Amanda Poole, M.Eng. is an environmental engineer at Baxter & Woodman, where she focuses on energy reduction and generation measures at wastewater treatment plants. Amanda has been involved in numerous wastewater treatment plant energy audits and aeration energy reduction projects throughout the Chicago area. Amanda received her B.S. and M.S. in Environmental Engineering from the University of Illinois in Urbana Champaign. She has been working in the water/wastewater sector for the past 3 years and awaits her P.E. licensure in December She is an active member of the Central States Water Environment Association. David Green, AAS EET joined Baxter & Woodman in 2008 as a Senior Systems Integrator. Dave s passion for automation and innovation led him to become the Automation Technical Director. He brings over 16 years of experience designing and providing unique solutions to Automated Systems Integration projects. He has quickly become a technical leader in the organization, and has a hunger for learning new technology and finding the best solutions for automation problems. Nick Camin, BSEE, MBA has worked in the instrumentation field for over thirteen years specializing in environmental industry applications for over ten of them. Nick is a graduate of Purdue University with a bachelor of sciences degree in electrical engineering and he also holds a master of business administration degree from Indiana Wesleyan University. With Endress+Hauser he has held the positions of application engineer, project manager, municipal business manager, regional sales manager and currently he is marketing manager for the environmental industry. Nick is a member of WEF and AWWA instrumentation and control committees.

SHOULD WE KEEP DO FOR NITRIFICATION CONTROL?

SHOULD WE KEEP DO FOR NITRIFICATION CONTROL? SHOULD WE KEEP DO FOR NITRIFICATION CONTROL? The proof is in the Ammonium Electrodes Standards Certification Education & Training Publishing Conferences & Exhibits Speaker: Robert Lagrange 2012 ISA Water

More information

Aeration System Automation: Controls Strategies to Maximize Energy Savings at Low Capital Cost

Aeration System Automation: Controls Strategies to Maximize Energy Savings at Low Capital Cost Aeration System Automation: Controls Strategies to Maximize Energy Savings at Low Capital Cost Amanda Poole, Jason Neighbors, David Green, Sue Baert, Chris Sosnowski, Derek Wold March 20, 2012 3:30 PM

More information

Advanced Control in Water and Wastewater Systems

Advanced Control in Water and Wastewater Systems Advanced Control in Water and Wastewater Systems Mandy Poole, P.E. Jason Neighbors Dave Green June 6, 2014 AGENDA What is a control loop? Control Theory Pump Control Levels of Control Case study on Wastewater

More information

Sensors for Activated Sludge Aeration Control

Sensors for Activated Sludge Aeration Control October 23, 2012 Use of Ammonia and Nitrate Sensors for Activated Sludge Aeration Control Troy Morgan; Western Regional Process Analytical Manager Overview Sensors Available Optical - Nitrate / Nitrite

More information

James Winslade Instructor, Environmental Resources Training Center Southern Illinois University-Edwardsville

James Winslade Instructor, Environmental Resources Training Center Southern Illinois University-Edwardsville James Winslade Instructor, Environmental Resources Training Center Southern Illinois University-Edwardsville In Memory of Steven Fiepke Chief Operator Village of Algonquin WWTP Skilled in Operation Dedicated

More information

Module 17: The Activated Sludge Process - Part III Answer Key

Module 17: The Activated Sludge Process - Part III Answer Key Module 17: The Activated Sludge Process - Part III Answer Key What other differences can you see between Complete Mix and Step Aeration? One of the features that make Complete Mix Aeration different from

More information

Presentation Outline

Presentation Outline Presentation Outline Nitrification/denitrification refresher Treatment technologies available for nitrification and BNR/ENR What is the problem? BNR/ENR VPDES permitting Causes of reduced BNR performance

More information

WASTEWATER TREATMENT PLANT MASTER PLAN 6. BUSINESS CASE EVALUATION OF ALTERNATIVES

WASTEWATER TREATMENT PLANT MASTER PLAN 6. BUSINESS CASE EVALUATION OF ALTERNATIVES WASTEWATER TREATMENT PLANT MASTER PLAN 6. BUSINESS CASE EVALUATION OF ALTERNATIVES A range of potential ammonia limits were identified for alternatives evaluation, as discussed in Section 2.2.5. This chapter

More information

Analytical Instrumentation for Wastewater Monitoring

Analytical Instrumentation for Wastewater Monitoring January 23, 2014 Analytical Instrumentation for Wastewater Monitoring ONLINE MONITORING FOR INDUSTRIAL WWT APPLICATIONS 1 Did you see this? It is sooo cold. 2 Rob Smith, P.E., BCEE, Ph.D. Applications

More information

Bioprocess Intelligent Operating System -Beyond Ammonia Control-

Bioprocess Intelligent Operating System -Beyond Ammonia Control- Bioprocess Intelligent Operating System -Beyond Ammonia Control- BioChem Technology, Inc. King of Prussia, PA May 20, 2015 Company Milestones 1978 Incorporation of BioChem Technology, Inc. as a pharmaceutical

More information

ENHANCING THE PERFORMANCE OF OXIDATION DITCHES. Larry W. Moore, Ph.D., P.E., DEE Professor of Environmental Engineering The University of Memphis

ENHANCING THE PERFORMANCE OF OXIDATION DITCHES. Larry W. Moore, Ph.D., P.E., DEE Professor of Environmental Engineering The University of Memphis ENHANCING THE PERFORMANCE OF OXIDATION DITCHES Larry W. Moore, Ph.D., P.E., DEE Professor of Environmental Engineering The University of Memphis ABSTRACT Oxidation ditches are very popular wastewater treatment

More information

W O C H H O L Z R E G I O N A L W A T E R R E C L A M A T I O N F A C I L I T Y O V E R V I E W

W O C H H O L Z R E G I O N A L W A T E R R E C L A M A T I O N F A C I L I T Y O V E R V I E W Facility Overview The recently upgraded and expanded Henry N. Wochholz Regional Water Reclamation Facility (WRWRF) treats domestic wastewater generated from the Yucaipa-Calimesa service area. The WRWRF

More information

SIMPLE and FLEXIBLE ENERGY SAVINGS And PERFORMANCE ENHANCEMENT for OXIDATION DITCH UPGRADES

SIMPLE and FLEXIBLE ENERGY SAVINGS And PERFORMANCE ENHANCEMENT for OXIDATION DITCH UPGRADES SIMPLE and FLEXIBLE ENERGY SAVINGS And PERFORMANCE ENHANCEMENT for OXIDATION DITCH UPGRADES Oxidation ditches are very popular wastewater treatment processes for small to medium sized municipalities that

More information

Increasing Denitrification in Sequencing Batch Reactors with Continuous Influent Feed

Increasing Denitrification in Sequencing Batch Reactors with Continuous Influent Feed Increasing Denitrification in Sequencing Batch Reactors with Continuous Influent Feed ABSTRACT In this study, the denitrification capacity of a continuous influent feed sequencing batch reactor (SBR) was

More information

CITY OF OXFORD WASTEWATER TREATMENT FACILITY ANNUAL PERFORMANCE REPORT FOR THE CALENDAR YEAR OF 2018

CITY OF OXFORD WASTEWATER TREATMENT FACILITY ANNUAL PERFORMANCE REPORT FOR THE CALENDAR YEAR OF 2018 CITY OF OXFORD WASTEWATER TREATMENT FACILITY ANNUAL PERFORMANCE REPORT FOR THE CALENDAR YEAR OF 2018 PREPARED: January 2019 2018 ANNUAL PERFORMANCE REPORT FOR THE CITY OF OXFORD WASTEWATER TREATMENT FICILITY

More information

City of Andover, Kansas Energy Assessment-Wastewater Treatment Plant

City of Andover, Kansas Energy Assessment-Wastewater Treatment Plant City of Andover, Kansas Energy Assessment-Wastewater Treatment Plant April 7, 2014 Prepared by Jerry Blain, P.E., Project Associate Environmental Finance Center Funding for this Energy Assessment was provided

More information

CITY OF OXFORD WASTEWATER TREATMENT FACILITY ANNUAL PERFORMANCE REPORT FOR THE CALENDAR YEAR OF 2014

CITY OF OXFORD WASTEWATER TREATMENT FACILITY ANNUAL PERFORMANCE REPORT FOR THE CALENDAR YEAR OF 2014 CITY OF OXFORD WASTEWATER TREATMENT FACILITY ANNUAL PERFORMANCE REPORT FOR THE CALENDAR YEAR OF 2014 PREPARED: January 2015 2014 ANNUAL PERFORMANCE REPORT FOR THE CITY OF OXFORD WASTEWATER TREATMENT FICILITY

More information

Integrated Fixed Film Activated Sludge (IFAS) System for Additional Nitrification at the Coldwater WWTP

Integrated Fixed Film Activated Sludge (IFAS) System for Additional Nitrification at the Coldwater WWTP Fishbeck, Thompson, Carr & Huber, Inc. Integrated Fixed Film Activated Sludge (IFAS) System for Additional Nitrification at the Coldwater WWTP Jim Flamming, P.E., Senior Process Engineer, FTC&H Dave Woodman,

More information

City of Elk River Wastewater Treatment Facility Improvements. Achieving Wastewater Treatment Goals

City of Elk River Wastewater Treatment Facility Improvements. Achieving Wastewater Treatment Goals City of Elk River Wastewater Treatment Facility Improvements Achieving Wastewater Treatment Goals By Tejpal Bala, P.E. Bolton & Menk, Inc. The City of Elk River received a new NPDES permit and the existing

More information

THE SEQUENCED AERATION PROCESS MONTAGUE, MASSACHUSETTS

THE SEQUENCED AERATION PROCESS MONTAGUE, MASSACHUSETTS THE SEQUENCED AERATION PROCESS MONTAGUE, MASSACHUSETTS GRANT WEAVER, PE & WASTEWATER OPERATOR THE WATER PLANET COMPANY WEBINAR APRIL 15, 2014 www.cleanwaterops.com Montague, Massachusetts 1.8 MGD Population

More information

On-Line Nutrient Monitoring-Operator s Job Got Easier

On-Line Nutrient Monitoring-Operator s Job Got Easier On-Line Nutrient Monitoring-Operator s Job Got Easier Viraj desilva, PhD, PE, BCEE American Structurepoint, Inc. June 24, 2015 2015 OWEA Conference - Sandusky, Ohio 1 Presentation Outline Introduction

More information

COMPARISON OF SBR AND CONTINUOUS FLOW ACTIVATED SLUDGE FOR NUTRIENT REMOVAL

COMPARISON OF SBR AND CONTINUOUS FLOW ACTIVATED SLUDGE FOR NUTRIENT REMOVAL COMPARISON OF SBR AND CONTINUOUS FLOW ACTIVATED SLUDGE FOR NUTRIENT REMOVAL Alvin C. Firmin CDM Jefferson Mill, 670 North Commercial Street Suite 201 Manchester, New Hampshire 03101 ABSTRACT Sequencing

More information

Performance Evaluation of the Moores Creek Advanced Water Resource Recovery Facility

Performance Evaluation of the Moores Creek Advanced Water Resource Recovery Facility Performance Evaluation of the Moores Creek Advanced Water Resource Recovery Facility Richard W. Gullick, Ph.D. Director of Operations Timothy Castillo Wastewater Manager Presented to the Albemarle County

More information

Chapter 2: Description of Treatment Facilities

Chapter 2: Description of Treatment Facilities 2020 Facilities Plan Treatment Report 2.1 Introduction Chapter 2: Description of Treatment Facilities This chapter defines the Milwaukee Metropolitan Sewerage District (MMSD) service area. It also describes

More information

Prepared by the Operation of Municipal Wastewater Treatment Plants Task Force of the Water Environment Federation

Prepared by the Operation of Municipal Wastewater Treatment Plants Task Force of the Water Environment Federation Operation of Municipal Wastewater Treatment Plants WEF Manual of Practice No. 11 Chapter 31 Aerobic Digestion Sixth Edition Prepared by the Operation of Municipal Wastewater Treatment Plants Task Force

More information

History of the Plant

History of the Plant History of the Plant Discharge began May 2008 Plant capacity as built 20 mgd Expansion capacity 30 mgd Beginning discharge approximately 5.5 6.0 mgd Currently discharging 7.5 mgd Activated Sludge treatment

More information

Energy Reduction and Nutrient Removal in WWTPs Using Feed- Forward Process Control

Energy Reduction and Nutrient Removal in WWTPs Using Feed- Forward Process Control Energy Reduction and Nutrient Removal in WWTPs Using Feed- Forward Process Control Tilo Stahl, Ph.D. 1 *, George Lee 1, Matthew Gray 1, P.E, Steven Kestel 1 1 BioChem Technology, Inc., King of Prussia,

More information

Aeration Blower Requirements. Tom Jenkins 06/15/2016

Aeration Blower Requirements. Tom Jenkins 06/15/2016 Aeration Blower Requirements Tom Jenkins 06/15/2016 Aeration blowers receive a lot of attention from design engineers, suppliers, and end users. That is understandable since blowers account for more than

More information

Operation and Control of Multiple BNR Processes in One WWTP

Operation and Control of Multiple BNR Processes in One WWTP Operation and Control of Multiple BNR Processes in One WWTP CENTRAL PLANT Williamsport Sanitary Authority s Chesapeake Bay and CSO Compliance Program Presented by: Phil Anderson 1 June 24, 2015 Purpose

More information

Making Your Plant Denitrify

Making Your Plant Denitrify Making Your Plant Denitrify Control the Process and Reap the Benefits Brett Ward Utility Operations Consultant Municipal Technical Advisory Service The University of Tennessee 1 Why Denitrify? Required

More information

AquaPASS. Aqua MixAir System. Phase Separator. System Features and Advantages. Anaerobic. Staged Aeration. Pre-Anoxic.

AquaPASS. Aqua MixAir System. Phase Separator. System Features and Advantages. Anaerobic. Staged Aeration. Pre-Anoxic. PHASED ACTIVATED SLUDGE SYSTEM PHASED ACTIVATED SLUDGE SYSTEM Aqua-Aerobic Systems has led the industry in time-managed, biological technology since 1984. In 2004, Aqua-Aerobic applied its expertise in

More information

CITY OF OXFORD WASTEWATER TREATMENT FACILITY ANNUAL PERFORMANCE REPORT FOR THE CALENDAR YEAR OF 2012

CITY OF OXFORD WASTEWATER TREATMENT FACILITY ANNUAL PERFORMANCE REPORT FOR THE CALENDAR YEAR OF 2012 CITY OF OXFORD WASTEWATER TREATMENT FACILITY ANNUAL PERFORMANCE REPORT FOR THE CALENDAR YEAR OF 2012 PREPARED: January 2013 2012 ANNUAL PERFORMANCE REPORT FOR THE CITY OF OXFORD WASTEWATER TREATMENT FICILITY

More information

Review of WEFTEC 2016 Challenge & Overview of 2017 Event. Malcolm Fabiyi, PhD, MBA Spencer Snowling, PhD. P.Eng

Review of WEFTEC 2016 Challenge & Overview of 2017 Event. Malcolm Fabiyi, PhD, MBA Spencer Snowling, PhD. P.Eng Review of WEFTEC 2016 Challenge & Overview of 2017 Event Malcolm Fabiyi, PhD, MBA Spencer Snowling, PhD. P.Eng Agenda Review 2016 Challenge Provide overview of updates to 2017 event Frequency WEFTEC Scores

More information

Ammonia Controlled Aeration. CSWEA 85 th Annual Conference. Don Esping, P.E. May 15, 2012

Ammonia Controlled Aeration. CSWEA 85 th Annual Conference. Don Esping, P.E. May 15, 2012 Ammonia Controlled Aeration CSWEA 85 th Annual Conference Don Esping, P.E. May 15, 2012 1 Ammonia Controlled Aeration Goals Reduced energy consumption Reduced total nitrogen Rieger, WEFTEC 2010 Brown and

More information

Optimizing Water Reclamation Systems by Automation using Continuous Water Quality Analysis

Optimizing Water Reclamation Systems by Automation using Continuous Water Quality Analysis Optimizing Water Reclamation Systems by Automation using Continuous Water Quality Analysis Standards Certification Education & Training Publishing Conferences & Exhibits Speakers: Vickie G. Olson, Honeywell

More information

Contents General Information Abbreviations and Acronyms Chapter 1 Wastewater Treatment and the Development of Activated Sludge

Contents General Information Abbreviations and Acronyms Chapter 1 Wastewater Treatment and the Development of Activated Sludge Contents Contents General Information Abbreviations and Acronyms... 6 Chapter 1 Wastewater Treatment and the Development of Activated Sludge... 8 The Importance of Wastewater Treatment... 8 The Scope of

More information

Advanced Optimization of Biological Nutrient Removal Plants Using Feedforward and Feedback Control-Case Studies

Advanced Optimization of Biological Nutrient Removal Plants Using Feedforward and Feedback Control-Case Studies Advanced Optimization of Biological Nutrient Removal Plants Using Feedforward and Feedback Control-Case Studies Rob Dexter*, Patrick Keller** and Rudolf Bauer** * DCM Process Control PTY Ltd. A.B.N. 89

More information

Online Organics Monitoring for Rapid Process Control of Drinking Water and Wastewater Treatment Operations

Online Organics Monitoring for Rapid Process Control of Drinking Water and Wastewater Treatment Operations Online Organics Monitoring for Rapid Process Control of Drinking Water and Wastewater Treatment Operations Amanda Scott Suez Water Technologies & Solutions 2018 ISA Water/Wastewater & Automatic Controls

More information

Post-Aerobic Digester with Bioaugmentation Pilot Study City of Meridian, ID WWTP PNCWA 2010

Post-Aerobic Digester with Bioaugmentation Pilot Study City of Meridian, ID WWTP PNCWA 2010 Post-Aerobic Digester with Bioaugmentation Pilot Study City of Meridian, ID WWTP by: William Leaf Adrienne Menniti Bruce Johnson CH2M HILL, Inc. Clint Dolsby Tracy Crane City of Meridian October 26, 21

More information

Dipankar Sen, PhD, PE Santa Clara Valley Water District Professor, Virginia Tech Civil & Env Engr

Dipankar Sen, PhD, PE Santa Clara Valley Water District Professor, Virginia Tech Civil & Env Engr Dipankar Sen, PhD, PE Santa Clara Valley Water District Professor, Virginia Tech Civil & Env Engr Outline Changes in wastewater in our industry How it affects the wastewater treatment plant Advanced Wastewater

More information

RTC-N: Modelling Ammonia-Based Aeration Control in Real Time for Deeper Process Control

RTC-N: Modelling Ammonia-Based Aeration Control in Real Time for Deeper Process Control RTC-N: Modelling Ammonia-Based Aeration Control in Real Time for Deeper Process Control By Bob Dabkowski, Application Development Manager, Hach Melody White, Application Development Manager, Hach Introduction

More information

RE ENGINEERING O&M PRACTICES TO GET NITROGEN & PHOSPHORUS REMOVAL WITHOUT FACILITY UPGRADES

RE ENGINEERING O&M PRACTICES TO GET NITROGEN & PHOSPHORUS REMOVAL WITHOUT FACILITY UPGRADES RE ENGINEERING O&M PRACTICES TO GET NITROGEN & PHOSPHORUS REMOVAL WITHOUT FACILITY UPGRADES GRANT WEAVER, PE & WASTEWATER OPERATOR WISCONSIN WASTEWATER OPERATORS ASSOCIATION WISCONSIN DELLS, WI OCTOBER

More information

Preparing for Nutrient Removal at Your Treatment Plant

Preparing for Nutrient Removal at Your Treatment Plant Summer Seminar Emerging Issues in the Water/Wastewater Industry Preparing for Nutrient Removal at Your Treatment Plant Rajendra P. Bhattarai, P.E., BCEE Austin Water Utility Ana J. Peña-Tijerina, Ph.D.,

More information

2015 ISA Water / Wastewater and Automatic Controls Symposium August 4-6, 2015 Orlando, Florida, USA

2015 ISA Water / Wastewater and Automatic Controls Symposium August 4-6, 2015 Orlando, Florida, USA Standards Certification Education & Training Publishing Conferences & Exhibits Utilizing Instrumentation and Control Tuning for BNR Optimization Speakers: Craig Fuller, AECOM Technical Services Norman

More information

Best Practice in Sewage and Effluent Treatment Technologies

Best Practice in Sewage and Effluent Treatment Technologies Best Practice in Sewage and Effluent Treatment Technologies Contents 1 Wastewater - Introduction 1 1.1 Earth s ecological system 1 1.1.1 Water effect on ecology 2 1.1.2 Wastewater generation 3 1.2 Wastewater

More information

THE DEMON ANAMMOX PROCESS: RESOURCE SAVINGS THROUGH SIDE STREAM TREATMENT, AND THE STEPS TOWARDS AN ENERGY NEUTRAL WWTP PRESENTED AT: NC AWWA-WEA 97

THE DEMON ANAMMOX PROCESS: RESOURCE SAVINGS THROUGH SIDE STREAM TREATMENT, AND THE STEPS TOWARDS AN ENERGY NEUTRAL WWTP PRESENTED AT: NC AWWA-WEA 97 THE DEMON ANAMMOX PROCESS: RESOURCE SAVINGS THROUGH SIDE STREAM TREATMENT, AND THE STEPS TOWARDS AN ENERGY NEUTRAL WWTP PRESENTED AT: NC AWWA-WEA 97 TH ANNUAL CONFERENCE PRESENTED ON: 13 NOVEMBER, 2017

More information

quality improvement and GHG reduction in

quality improvement and GHG reduction in New approaches to the coexistence of water quality improvement and GHG reduction in wastewater treatment Challenges of the Bureau of Sewerage, Tokyo Metropolitan Government toward the shift in operation

More information

NITROGEN REMOVAL OPTIMISATION FROM COMPLEX WASTEWATER

NITROGEN REMOVAL OPTIMISATION FROM COMPLEX WASTEWATER NITROGEN REMOVAL OPTIMISATION FROM COMPLEX WASTEWATER D.D. Irvine and A. Khan Pattle Delamore Partners Limited, Auckland, New Zealand A.F. Findson Wallace Corporation Limited, Waitoa, New Zealand ABSTRACT

More information

Nutrient Removal Optimization at the Fairview WWTP

Nutrient Removal Optimization at the Fairview WWTP Alyssa Mayer, PE Principal Engineer Nutrient Removal Optimization at the Fairview WWTP Mark Strahota, PE Associate Presentation Overview Project Background Process Model Development BNR Design Considerations

More information

The oxidation index: a tool for controlling the activated sludge process

The oxidation index: a tool for controlling the activated sludge process The oxidation index: a tool for controlling the activated sludge process A common approach to controlling the activated sludge process involves adjusting the amount of biomass in the system according to

More information

American Water College 2010

American Water College 2010 Vocabulary Activated Sludge (Part 1) Activated Sludge Sludge particles produced in raw or settled wastewater (primary effluent) by the growth of organisms (including zoogleal bacteria) in aeration tanks

More information

Secondary Treatment Process Control

Secondary Treatment Process Control SARBS One-Day Training Seminar Phoenix Club, Anaheim Secondary Treatment Process Control Graham Juby June 5, 2013 Objectives Provide an understanding of nitrogen removal process interactions to support

More information

Energy Savings Through Denitrification

Energy Savings Through Denitrification Energy Savings Through Denitrification If Your Plant Nitrifies, Why Not Make it Denitrify Brett Ward Utility Operations Consultant Municipal Technical Advisory Service The University of Tennessee 1 Nitrate,

More information

EXPRESS TERMS: Existing Part 650 is repealed in its entirety and New Part 650 is adopted.

EXPRESS TERMS: Existing Part 650 is repealed in its entirety and New Part 650 is adopted. EXPRESS TERMS: Existing Part 650 is repealed in its entirety and New Part 650 is adopted. Chapter X Division of Water Resources PART 650 Qualifications of s of Wastewater Treatment Plants Statutory authority:

More information

At the Mercy of the Process Impacts of Nitrogen Removal Performance on WWTP Disinfection

At the Mercy of the Process Impacts of Nitrogen Removal Performance on WWTP Disinfection OBG PRESENTS: At the Mercy of the Process Impacts of Nitrogen Removal Performance on WWTP Disinfection Ned Talbot, PE Tri-Association Conference 2018 8/30/18 9:00-9:30AM AGENDA Overview of Plant Processes

More information

Upgrading Lagoons to Remove Ammonia, Nitrogen, and Phosphorus *nutrient removal in cold-climate lagoon systems

Upgrading Lagoons to Remove Ammonia, Nitrogen, and Phosphorus *nutrient removal in cold-climate lagoon systems Upgrading Lagoons to Remove Ammonia, Nitrogen, and Phosphorus *nutrient removal in cold-climate lagoon systems October 7, 2015 3:15 4:00pm Session M Room Tamboti / Aloes-wood Treatment Processes Aerated

More information

Walter E. Deuchler Associates, Inc. Consulting Engineers

Walter E. Deuchler Associates, Inc. Consulting Engineers I. DESCRIPTION OF PROJECT HIGHLIGHTS P lanning for the latest improvements to the Salt Creek Sanitary District (District) began in 2001 with the updating of the Facility Plan, which identified the need

More information

Aeration University Advanced Concepts in Energy Efficiency

Aeration University Advanced Concepts in Energy Efficiency Aeration University Advanced Concepts in Energy Efficiency Wisconsin Wastewater Operators Association 47 th Annual Conference October 23, 2013 Presented by Phil Korth Aeration and Energy Wastewater Treatment

More information

2015 HDR, Inc., all rights reserved.

2015 HDR, Inc., all rights reserved. 2015 HDR, Inc., all rights reserved. Hastings Utilities Water Pollution Control Facility Improvements Brian Bakke, HDR ASCE Environmental Conference 4/6/2017 Review Existing Facilities Need for the Project

More information

NITROGEN REMOVAL GUIDE FOR WASTEWATER OPERATORS THE WATER PLANET COMPANY FORMS OF NITROGEN OF INTEREST TO WASTEWATER OPERATORS

NITROGEN REMOVAL GUIDE FOR WASTEWATER OPERATORS THE WATER PLANET COMPANY   FORMS OF NITROGEN OF INTEREST TO WASTEWATER OPERATORS NITROGEN REMOVAL GUIDE FOR WASTEWATER OPERATORS THE WATER PLANET COMPANY www.cleanwaterops.com FORMS OF NITROGEN OF INTEREST TO WASTEWATER OPERATORS Nitrogen exists in several forms. The principal nitrogen

More information

20 Years of Nutrient Removal City of Beloit

20 Years of Nutrient Removal City of Beloit 20 Years of Nutrient Removal City of Beloit Leon Downing, PhD, PE, & Bill Marten, PE, BCEE Donohue Harry Mathos & Nate Tillis City of Beloit IWEA Nutrient Removal and Recovery Workshop September 12, 2013

More information

NITROGEN REMOVAL GRANT WEAVER, PE & WWTP OPERATOR PRESIDENT THE WATER PLANET COMPANY. Create Optimal Habitats

NITROGEN REMOVAL GRANT WEAVER, PE & WWTP OPERATOR PRESIDENT THE WATER PLANET COMPANY.   Create Optimal Habitats NITROGEN REMOVAL Create Optimal Habitats Recognize the Importance of People Skills Full-scale Experimentation GRANT WEAVER, PE & WWTP OPERATOR Regulatory Support Utility Support PRESIDENT THE WATER PLANET

More information

Aqua MSBR MODIFIED SEQUENCING BATCH REACTOR

Aqua MSBR MODIFIED SEQUENCING BATCH REACTOR MODIFIED SEQUENCING BATCH REACTOR MODIFIED SEQUENCING BATCH REACTOR For over three decades, Aqua-Aerobic Systems has led the industry in sequencing batch reactor technology with performance proven and

More information

Altoona Westerly Wastewater Treatment Facility BNR Conversion with Wet Weather Accommodation

Altoona Westerly Wastewater Treatment Facility BNR Conversion with Wet Weather Accommodation Pennsylvania Water Environment Federation PennTEC Annual Technical Conference June 4, 2013 Altoona Westerly Wastewater Treatment Facility BNR Conversion with Wet Weather Accommodation Presented by: Jim

More information

CLR Process. Vertical Loop Configuration

CLR Process. Vertical Loop Configuration CLR Process Vertical Loop Configuration Vertical Configuration System Flexibility Parallel Operation Raw wastewater and return activated sludge are introduced at a single point in each standard CLR basin.

More information

City of Oregon Wastewater Treatment Plant (WWTP) Secondary Treatment Improvement Project Phases 1 & 2 FAQ Sheet

City of Oregon Wastewater Treatment Plant (WWTP) Secondary Treatment Improvement Project Phases 1 & 2 FAQ Sheet City of Oregon Wastewater Treatment Plant (WWTP) Secondary Treatment Improvement Project Phases 1 & 2 FAQ Sheet WHY IS THE CITY OF OREGON DOING THIS PROJECT? Along with other communities across the country,

More information

WASTEWATER DEPARTMENT. Bentonville Wastewater Treatment Plant Facts:

WASTEWATER DEPARTMENT. Bentonville Wastewater Treatment Plant Facts: Mission: The mission of the Bentonville Wastewater Treatment Utility and staff is to protect public health and the environment through the effective treatment of wastewater. Effective wastewater treatment

More information

Aeration Basics the Bug s Eye View

Aeration Basics the Bug s Eye View Aeration Basics the Bug s Eye View Leonard E. Ripley, Ph.D., P.E., BCEE Senior Environmental Engineer Freese and Nichols, Inc. WEAT Electrical & Instrumentation Seminar March 20, 2019 Why Do We Aerate?

More information

From manual to automatic at Spring Creek

From manual to automatic at Spring Creek When upgrading its water resource recovery facility on Spring Creek, the Springfield (Ill.) Metro Sanitary District designed with operations in mind. By bringing together operators and designers, the district

More information

NEW BIOLOGICAL PHOSPHORUS REMOVAL CONCEPT SUCCESSFULLY APPLIED IN A T-DITCH PROCESS WASTEWATER TREATMENT PLANT

NEW BIOLOGICAL PHOSPHORUS REMOVAL CONCEPT SUCCESSFULLY APPLIED IN A T-DITCH PROCESS WASTEWATER TREATMENT PLANT NEW BIOLOGICAL PHOSPHORUS REMOVAL CONCEPT SUCCESSFULLY APPLIED IN A T-DITCH PROCESS WASTEWATER TREATMENT PLANT ABSTRACT C. Yang*, L. Zhou**, W. Luo***, and L. Johnson**** *Corstar International Corp. 111

More information

Operations Report. September 10, 2015

Operations Report. September 10, 2015 Operations Report September 1, 215 Plant Loading and Operations Summary August 215 Biochemical Oxygen Demand, 5-Day (Avg. 2,151 lb./day) Total Suspended Solids (Avg. 33,197 lb./day) Average Daily Flow

More information

Copies: Mark Hildebrand (NCA) ARCADIS Project No.: April 10, Task A 3100

Copies: Mark Hildebrand (NCA) ARCADIS Project No.: April 10, Task A 3100 MEMO To: Jeff Pelz (West Yost) Kathryn Gies (West Yost) Copies: Mark Hildebrand (NCA) ARCADIS U.S., Inc. 200 Harvard Mills Square Suite 430 Wakefield Massachusetts 01880 Tel 781 224 4488 Fax 781 224 3033

More information

General Information on Nitrogen

General Information on Nitrogen General Information on Nitrogen What is nitrogen? Nitrogen was discovered in 1772 by Daniel Rutherford in Scotland Nitrogen gas makes up nearly 80% of the air we breathe Nitrogen gas is not toxic Nitrogen

More information

TWO YEARS OF BIOLOGICAL PHOSPHORUS REMOVAL WITH AN ADVANCED MSBR SYSTEM AT THE SHENZHEN YANTIAN WASTEWATER TREATMENT PLANT

TWO YEARS OF BIOLOGICAL PHOSPHORUS REMOVAL WITH AN ADVANCED MSBR SYSTEM AT THE SHENZHEN YANTIAN WASTEWATER TREATMENT PLANT TWO YEARS OF BIOLOGICAL PHOSPHORUS REMOVAL WITH AN ADVANCED MSBR SYSTEM AT THE SHENZHEN YANTIAN WASTEWATER TREATMENT PLANT Chester Yang, Ph.D., Gaowei Gu, Baowei Li, Hongyuan Li, Wanshen Lu, Lloyd Johnson,

More information

MUNICIPALITY OF WEST ELGIN RODNEY WASTEWATER TREATMENT PLANT

MUNICIPALITY OF WEST ELGIN RODNEY WASTEWATER TREATMENT PLANT MUNICIPALITY OF WEST ELGIN RODNEY WASTEWATER TREATMENT PLANT 214 ANNUAL REPORT uary 1 to ember 31, 214 Environmental Compliance Approval # 3-871-88-949 Prepared by: Table of Contents Section 1: Overview...

More information

UPGRADING FOR TOTAL NITROGEN REMOVAL WITH A POROUS MEDIA IFAS SYSTEM

UPGRADING FOR TOTAL NITROGEN REMOVAL WITH A POROUS MEDIA IFAS SYSTEM UPGRADING FOR TOTAL NITROGEN REMOVAL WITH A POROUS MEDIA IFAS SYSTEM T. Masterson, J. Federico, G. Hedman, S. Duerr BETA Group, Inc. 6 Blackstone Valley Place Lincoln, Rhode Island 02865 ABSTRACT The Westerly,

More information

RESULTS OF ECOSYSTEMS PLUS INJECTION IN SECONDARY AERATION LAGOONS

RESULTS OF ECOSYSTEMS PLUS INJECTION IN SECONDARY AERATION LAGOONS RESULTS OF ECOSYSTEMS PLUS INJECTION IN SECONDARY AERATION LAGOONS GLOBAL FOOD MANUFACTURER (SEPTEMBER 6-22 2006) PRIMARY PROJECT OBJECTIVES: Demonstrate ESP 's ability to increase the transfer of dissolved

More information

Process Monitoring for Biological and Chemical Nutrient Removal

Process Monitoring for Biological and Chemical Nutrient Removal October 27, 2016 Process Monitoring for Biological and Chemical Nutrient Removal OWEA 2016 PLANT OPERATIONS & LABORATORY WORKSHOP Agenda Why Consider Nutrient Removal? Nitrogen Monitoring & Removal Phosphorus

More information

Proprietary AquaTron technology incorporates three (3) innovative features that increase its efficiency and reduces cost:

Proprietary AquaTron technology incorporates three (3) innovative features that increase its efficiency and reduces cost: THE AQUATRON The Technology The AquaTron is the result of over twenty years of research, development, testing and practical experience. Using the principles of the activated sludge biological process,

More information

Ditches for Energy Efficiency and Improved Nitrogen Removal

Ditches for Energy Efficiency and Improved Nitrogen Removal Upgrade of the Big Gulch WWTP Oxidation Ditches for Energy Efficiency and Improved Nitrogen Removal Thomas G. Authors: Thomas E. Coleman, dtec Systems Bridges, Mukilteo Water & Wastewater District Bend,

More information

Case Study. Biological Help for the Human Race. BiOWiSH Aqua Improves Nutrient Removal in a Wastewater Treatment Plant - Oberon, Australia

Case Study. Biological Help for the Human Race. BiOWiSH Aqua Improves Nutrient Removal in a Wastewater Treatment Plant - Oberon, Australia Case Study BiOWiSH Aqua BiOWiSH Aqua Improves Nutrient Removal in a Wastewater Treatment Plant - Oberon, Australia BiOWiSH Aqua Executive Summary A bioaugmentation program using BiOWiSH Aqua was implemented

More information

BEING GOOD STEWARDS: IMPROVING EFFLUENT QUALITY ON A BARRIER ISLAND. 1.0 Executive Summary

BEING GOOD STEWARDS: IMPROVING EFFLUENT QUALITY ON A BARRIER ISLAND. 1.0 Executive Summary BEING GOOD STEWARDS: IMPROVING EFFLUENT QUALITY ON A BARRIER ISLAND Brett T. Messner, PE, Tetra Tech, Inc., 201 E Pine St, Suite 1000, Orlando, FL 32801 Brett.Messner@tetratech.com, Ph: 239-851-1225 Fred

More information

SBR PROCESS FOR WASTEWATER TREATMENT

SBR PROCESS FOR WASTEWATER TREATMENT SBR PROCESS FOR WASTEWATER TREATMENT IMR E&T S.r.l. Maria Vittoria Marra maria.vittoria.marra@imr.it www.imr.it Purification of wastewater A process aimed at removing organic and inorganic contaminants

More information

Refinement of Nitrogen Removal from Municipal Wastewater Treatment Plants

Refinement of Nitrogen Removal from Municipal Wastewater Treatment Plants Refinement of Nitrogen Removal from Municipal Wastewater Treatment Plants Prepared for Maryland Department of the Environment Presented by: Gannett Fleming, Inc. Stephen B. Gerlach, PE & Carrie DeSimone

More information

Hybrid Sequencing Batch Reactors (SBR) Offer an Efficient Wastewater Treatment

Hybrid Sequencing Batch Reactors (SBR) Offer an Efficient Wastewater Treatment Hybrid Sequencing Batch Reactors (SBR) Offer an Efficient Wastewater Treatment CONTRIBUTING WRITERS Michael Lahlou, E.I.T. and James Matthews, P.E. Batch processes are not a new or innovative wastewater

More information

AquaNereda Aerobic Granular Sludge Technology

AquaNereda Aerobic Granular Sludge Technology Aerobic Granular Sludge AquaNereda Aerobic Granular Sludge Technology The AquaNereda Aerobic Granular Sludge (AGS) Technology is an innovative biological wastewater treatment technology that provides advanced

More information

BIOLOGICAL WASTEWATER BASICS

BIOLOGICAL WASTEWATER BASICS BIOLOGICAL WASTEWATER BASICS PRESENTATION GOALS EXPLAIN DIFFERENT TYPES OF WASTEWATER EXPLAIN THE DIFFERENT BIOLOGICAL SYSTEMS AND HOW THEY FUNCTION. COMPARE AND CONTRAST AEROBIC AND ANAEROBIC SYSTEMS

More information

MUNICIPALITY OF WEST ELGIN WEST LORNE WASTEWATER TREATMENT PLANT

MUNICIPALITY OF WEST ELGIN WEST LORNE WASTEWATER TREATMENT PLANT MUNICIPALITY OF WEST ELGIN WEST LORNE WASTEWATER TREATMENT PLANT 214 ANNUAL REPORT uary 1 to ember 31, 214 Environmental Compliance Approval # 3-442-9-938 Prepared by: Table of Contents Section 1: Overview...

More information

SECTION 8.0 NEWPCC SECOND PRIORITY CONTROL ALTERNATIVES

SECTION 8.0 NEWPCC SECOND PRIORITY CONTROL ALTERNATIVES SECTION 8.0 NEWPCC SECOND PRIORITY CONTROL ALTERNATIVES 8.1 PREAMBLE Table 8.1 below indicates the target ammonia concentrations for the Best Practicable and the Second Priority Levels of Control for the

More information

2015 Spring Conference

2015 Spring Conference 2015 Spring Conference Meeting Strict Summer Permit Requirements on Day One: Start-up of the Western Wake Regional Water Reclamation Facility Chris White, PE April 13, 2015 Acknowledgements Town of Cary

More information

Chapter 5: Treatment Assessment Future Condition

Chapter 5: Treatment Assessment Future Condition 2020 Facilities Plan Treatment Report 5.1 Introduction Chapter 5: Treatment Assessment Future Condition The future performance of the Milwaukee Metropolitan Sewerage District (MMSD) wastewater treatment

More information

An Innovative Approach to Retrofitting for Nitrogen Removal

An Innovative Approach to Retrofitting for Nitrogen Removal June 29, 2017 An Innovative Approach to Retrofitting for Nitrogen Removal OWEA 2017 TECHNICAL CONFERENCE & EXPO Innovation From Wikipedia: The application of better solutions that meet new requirements.

More information

RE: Annual Report 2016 Wardsville Wastewater Treatment Plant and Collection System

RE: Annual Report 2016 Wardsville Wastewater Treatment Plant and Collection System 14 th, 217 Tom Clubb 3232 White Oak Road, 3 rd Floor London ON N6E 1L8 Attention: Mr. Clubb RE: Annual Report 216 Wardsville Wastewater Treatment Plant and Collection System The Ontario Clean Water Agency

More information

2017 Annual Performance Report

2017 Annual Performance Report Newcastle Water Pollution Control Plant The Regional Municipality of Durham Newcastle Water Pollution Control Plant Environmental Compliance Approval (ECA): 3-2189-87-946 Dated July 26, 1994 Amendments:

More information

Simultaneous Nutrient Removal: Quantification, Design, and Operation. Leon Downing, Ph.D., PE Donohue & Associates

Simultaneous Nutrient Removal: Quantification, Design, and Operation. Leon Downing, Ph.D., PE Donohue & Associates Simultaneous Nutrient Removal: Quantification, Design, and Operation Leon Downing, Ph.D., PE Donohue & Associates Simultaneous Nutrient Removal Simultaneous nitrification, denitrification, and potentially

More information

Pavel Hajda, Ph.D., P.E., Symbiont

Pavel Hajda, Ph.D., P.E., Symbiont Pavel Hajda, Ph.D., P.E., Symbiont 1. 2011 IAWA Nutrient Study 2. Supplemental analysis 3. Other efforts 4. Conclusions 1. Identify technologies widely applicable to P and/or N removal upgrades 2. Assess

More information

2017 Annual Performance Report

2017 Annual Performance Report 2017 Annual Performance Report Thornbury Wastewater Treatment Plant and Associated Collection System Prepared by: Wastewater Operations Staff Reporting Period: January 1 December 31, 2017 1 P age Executive

More information

This document can be made available in other accessible formats as soon as practicable and upon request. Staff Report. Infrastructure & Public Works

This document can be made available in other accessible formats as soon as practicable and upon request. Staff Report. Infrastructure & Public Works This document can be made available in other accessible formats as soon as practicable and upon request Staff Report Infrastructure & Public Works Report To: Committee of the Whole Meeting Date: March

More information

Using Process Optimization and Energy Audits to Reduce Energy Costs

Using Process Optimization and Energy Audits to Reduce Energy Costs Using Process Optimization and Energy Audits to Reduce Energy Costs PNCWA Annual Conference 23 October 2012 Ron Moeller Operations Services Leader Presentation Outline What is a process energy-audit? Energy

More information

LEITGIRIAI VILLAGE PILOT (LITHUANIA)

LEITGIRIAI VILLAGE PILOT (LITHUANIA) LEITGIRIAI VILLAGE PILOT (LITHUANIA) MIDONA DAPKIENĖ 04 10 2017, Warsaw LEITGIRIAI VILLAGE 2 Leitgiriai is a village with 104 inhabitants (40 households) in the district of Šilutė, near Leitė River (right

More information